Thursday, November 15, 2012

Ethanol and Emissions Control Functionality

In this article, I want to address the effects of stiff gasohol blends (exceeding 10 or 15% ethanol) on the functionality of aged catalytic converters. The materials compatibility and corrosion effects I have discussed in prior articles. I have discussed effects on power and mileage in prior articles. I have also discussed full E-85 conversions and those results in prior articles. You can navigate by date and title to see those articles very quickly using the tool on the left. That list, by date- title-content, is:

12-15-09 Red Letter Day: Ethanol VW Experiment Complete Presents a results summary for the “ethanol VW” as modified to run on full E-85. It documents the factor 1.15-1.20 increase in power and thermal efficiency relative to plain gasoline. It also documents the actual loss of fuel mileage (82% of gasoline), which is not in proportion to fuel heating value ratio (71%).

11-12-10 Stiff Blend Effects in Gasoline Cars Presents the effects of stiff blends in the former (full E-85) “ethanol VW” compared to the same stiff blends in an unmodified fuel-injected Ford F-150. The data demonstrates that there is approximately an E-40 limit for unmodified in fuel-injected engines, and that mileage with lesser blends is statistically indistinguishable from mileage on plain gasoline. A maximum of E-35 is recommended to avoid harmless but irritating cold start misbehavior.

11-17-10 Nissan Mileage Results on Blends The article reports finding the same blend limit of about E-40 in the unmodified fuel-injected Nissan. Mileage on lesser blends is essentially identical to mileage on plain gasoline. The results are identical to those of the Ford F-150.

2-12-11 “How-To” For Ethanol and Blend Vehicles This articles presents generalized “how-to” for doing your own E-85 conversions, and for running your own stiff gasohol blends in unmodified fuel-injected engines. There are 3 items to address in modern automotive conversions: mixture ratio, ignition timing, and extra intake heat. Slow-turning “under-square” engines in antique farm tractors, and airplanes, are insensitive to the timing issue. The only issues to address for stiff blends in unmodified vehicles are calculating the E-number from the fractions of E-85 and gasoline, and “calibrating” the marks on the fuel gage.

5-5-11 Ethanol Does Not Hurt Engines This article discusses actual experience with materials compatibility and fuel system housekeeping issues. It debunks some still-widely circulated myths. With the exceptions of Plexiglas and Lexan, and the antique pot-metal castings and lacquered cork floats, “if it’s good for gasoline, it’s good for ethanol” is a pretty good rule of thumb. The vast majority of the small engine troubles widely reported trace directly to pre-existing dirt and massive water bottoms in fuels systems. These get mobilized suddenly when ethanol enters the mix and cause problems in fuel metering devices, not the engines themselves. Those contaminants should not have been in there in the first place, for any decently-maintained and operated equipment.

8-9-12 Biofuels in General and Ethanol in Particular Presents a further (repeat) debunking of myths about ethanol in actual motors. This was in response to a published newspaper article circulating those same myths. Covers the engine damage myths and the low fuel mileage myths.

The vehicle in this article is the same Nissan that was reported in the 11-17-10 article. It is a 1998 Sentra with the GA-16 1.6 liter 4 cylinder engine, and automatic transmission. It was my wife’s car for several years. Once I started driving it, I began the blend experiments. I recently had the engine overhauled, which “calibrated” my best guess as to its design life. That overhaul also corrected a long-term chronic oil leak through the front seal. This was a “real-world” flawed machine, as are all the other vehicles in the other articles. See Fig. 1.


Figure 1 – The “Gasohol Nissan”

We bought the car used 6-1-99 with 15,560 miles on the odometer. It was clean, and seemed to be in good condition. It drove well and got good mileage. I did all the routine maintenance such as oil changes over all the years we have had this car. I used Castrol 20W-50 oil in it. A new distributor rotor fixed an ignition “no fire” failure at 42,707 miles. The oil leak started about 53,705 miles, when we fixed an exhaust leak. Remarkably, my records indicate no transmission repairs at all, just routine fluid and filter changes.

This car began experiencing failed starts December 2002 at odometer 70,360. These were erratically recurrent, and I finally traced them to weak dry compression (worn rings). The “fix” that I used for a long time was to squirt about a teaspoon or two of motor oil into each cylinder, which raised compression just enough for the control chip’s cold start mixture settings to actually ignite. As this condition worsened with age, it became necessary to open the throttle while cranking to raise compressed pressures sufficiently.

Minor items included a wiper linkage repair November 2004 at 96,286 miles, and replacement of a plugged PCV valve September 2005 at 105,993 miles. I re-rigged the crankcase ventilation to an overboard dump November 2006 at 123,410 miles in order to lower crankcase pressures as a means to slow the worsening oil leak. It was basically ineffective.

In June 2007 at 137,977 miles, I started adding Lucas Oil Stabilizer to the crankcase oil charge, in another effort to slow the oil leak through the seal. This stuff also has the effect of greatly arresting cold start wear, and raising the dry test compression pressures by more effectively sealing the worn rings. My erratic cold start failure problem essentially went away. I started about 19% additive, and worked up to 50% additive by about 140,000 miles, finding it minimally effective at slowing the oil leak rate. Slowing down actually helped more.

There was a “breakdown” requiring a tow and repairs May 2007 at 136,398 miles, due to water ingestion in street flooding in Beaumont. It did require a new alternator. I replaced the starter March 2008 at about 156,733 miles, and the first front axle / CV joint assembly about June 2008 at 159,230 miles. The transmission-side fan on the radiator required replacement about July 2008 at 160,806 miles. This flurry of significant repairs suggests that the intended life of the vehicle was about 150,000 miles. Such a design life would be consistent with a minimally-compliant catalytic converter designed to last at least 150,000 miles under the federal motor vehicle standards.

I had the engine drive belts replaced July 2009 at 185,297 miles, and had to repair the battery cable assemblies soon after. That was about the time we bought my wife a Toyota Prius, and I started driving the Nissan. I “calibrated” the gas gage marks and characterized fuel mileage on gasoline over the commute driving cycle to TSTC and back. I got all this done by late August 2009, at 186,489 miles. After that, I started driving the car on various “stiff” gasohol blends made by splash-blending E-85 and unleaded regular in the tank. I did add a Schrader fitting to the fuel line so I could test my blends with samples drawn from the feed to the fuel rail. That is the only modification I ever made. See fig. 2.


Figure 2 – Schrader fitting added to fuel line (next to brake fluid reservoir)

I had to replace the instrument cluster when the odometer failed October 2009 at about 188,000 miles. This, too, is evidence the design life of the car was closer to 150,000 miles. Best estimate is that I replaced the cluster at 188,605 miles, based on driving over distances that I knew well. The new cluster was a slightly-used part, and had 28,291 on it. The correction factor to original miles is thus replacement odometer reading + 160,314 = original miles. I replaced both drive axles and hubs, plus brake rotors August 2011 at 210,641 original miles. The crankcase leak got really bad that same month.

It was December 2011 at 214,424 original miles that I had the engine torn down and overhauled. That front seal was literally gone: an open annular hole. The main and rod bearings were “down to the red metal”, and the chain tensioner had been worn out, eroded completely through its phenolic layer. The timing chain was literally cutting steel from the back plate.

It was a full overhaul: new rings and pistons, reamed cylinders, new bearings, and a regrind on the crank, plus new oil and water pumps. The existing distributor, air conditioner, alternator and starter were retained. This engine had definitely been operated past its useful life, and was mere hours from throwing a rod. I believe with very good reasons that the intended design life was closer to 150,000 miles than the 214,000 miles I achieved. I believe that the only reason it went that far was because of the heavy usage of Lucas additive, which sharply reduced cold start wear. With the new tight bearings, I am using 5W-30 oil now, with no additive yet.

I replaced the EGR valve, and repaired the wiper linkage again in June-July 2012, around 220,000 original miles. June 27 2012 at 220,207 was my first check engine light with “catalytic converter not working” as the code. I replaced the other cooling fan on the radiator August 2012 at 221,827 miles. The pattern with the “catalytic converter not working” codes proved to be very interesting. If I ran plain gasoline (really E-10 gasohol these days), the check engine light would come on within days. About a week after returning to nominal E-30 blends, the light would go out. That pattern and otherwise good drivability continues to this publication date: November 15, 2012, at 225,196 miles.

My interpretation of this pattern of catalytic converter behavior is very simple: the E-10 they sell as regular gasoline is almost as sooty-burning a fuel as plain gasoline. My stiff blends ranged from E-20 to over E-40, usually E-30 plus or minus 5 points. That’s a lot more ethanol in the mix, which burns with a soot-free flame alone. Catalytic converters usually fail due to soot plugging or coating. Soot is inevitable in the exhaust system. It simply cannot all burn quickly enough in the cylinder before the exhaust valve opens. No solid fuel material can.

Running a stiff blend means there less soot in the flame, so there is less soot sent into the exhaust system to contaminate the converter. Further, there is a solvent action of the ethanol in the flame that acts to strip off carbon deposits somewhat. This would also help clean the converter of soot deposits to one extent or another.

I started using stiff gasohol blends at 186,489 miles, which is way past the apparent design life of the car and engine (about 150,000 miles or so). I am surprised the “converter not working” code did not appear sooner, but I first saw one using the occasional tank of plain gasoline at about 220,207 miles. To this day, that light goes out, indicating the converter resumes working, within about a week of filling with a nominal E-30 blend.

The petroleum fuel lobbies have convinced the EPA that blends “stiffer” than E-10 might harm emissions equipment. That’s why approval for E-15 has been delayed so long, and with recent-model restrictions so severe that we will likely never see it offered at most filling stations.

But, in direct contradiction to this, my experience strongly suggests that “stiff” ethanol blends actually extend catalytic converter life, by literally cleaning out some of the soot that “kills” them.

My F-150 pickup also has over 200,000 miles on it, and has been running E-30-something blends for almost 7 years now. Its tailpipe is clean as a whistle: bare steel. It used to be a bit sooty before I started using stiff ethanol blends. It will be very interesting to see how long that catalytic converter lasts. My Nissan experience suggests it will last a very long time yet: the design life of those pickups is reputed to be far longer than the Nissan’s apparent 150,000 miles-or-so.

Thursday, November 1, 2012

About the Kactus Kicker

Update 7-30-15:  The new website is fully operational.  It has all the information,  photos,  and videos anyone could ever need.  It is a turnkey site for selecting,  customizing,  and purchasing a production tool.  Shipping is available,  so sales of plans have been discontinued.  Some additional parts and labor have been farmed out to appropriate vendors,  to adjust to higher production rates,  so prices posted previously are now obsolete.  Go to http://www.killyourcactusnow.com

Update 3-1-18:  the killyourcactusnow site has been shut down in favor of a new and improved site http://howtokillcactus.com,  with even better information,  photos,  and videos.  

This article, plus an earlier one dated 12-28-2011, should give most prospective customers a good idea of what my cactus tool looks like, and how it is handled. This is a tool for the killing (eradication) of prickly pear cactus from pasture land. The key things to understand for handling the tool are how to pin the tow bridle into a lift sling, and how to pry up and prop the front for storage or debris removal. The tow bridle must be unpinned into the big V-shaped configuration for actual use in the pasture.

Transport from place to place is easy: a pickup or flat bed trailer is adequate. Your modern tractor's bucket can be used to hoist up the tool for loading and unloading. (Us old guys with antique tractors that have no bucket use a tree limb and a chain hoist.)

The CCT-002 “Kactus Kicker” cactus control tool is a drag-type farm implement somewhat similar to a simple plow, a hay rake, or a drag-type shredder. The cactus tool has no moving parts, and mechanically kills prickly pear cactus by running over the top of it, tearing it loose, and crushing it thoroughly, so that it bleeds out dry before it can re-root. It is not an earth-mover or grader-plow.

The tool is towed on a chain bridle that fits almost any kind of hitch. Typical tow loads in usage are around half a ton per tool. If used with a three-point hitch, care should be taken to ensure the hitch is braced to resist half-ton side loads per tool: these occur during turns. The tow bridle can be pinned into a lift sling with a single bolt (see below).

The tool comprises a 2-foot by 8-foot ¼-inch deck plate arranged to “cut” an 8-foot swath behind the tractor, a crushing rail at the back edge made of scrap railroad rail, a ballast bar at the rear, a “barge front” surface to wedge the tool over small rock outcrops, and a stabilizing “snout” that maintains the leading-edge geometry relative to the earth. Shipping dimensions and weights are as depicted in fig. 1:

Figure 1. -- Shipping Dimensions and Weights

The tool is of stick-welded construction, from standard sizes of plate, flat, tube, and angle. The railroad rail can be of any size from 4 to 6 inches tall; scrap is less expensive. The current configuration uses 4.5 inch tall rail, weighing 70.1 pounds per linear yard. The photo in fig. 2 shows a welded assembly being moved with a hoist (and temporary chain sling) outside for painting and rigging.

Figure 2. -- Finished Weld Assembly

The tool is painted on all upper surfaces and over all weld beads on upper or lower surfaces, with oil-based red implement paint, available from any hardware store. Fundamentally, the only need is to prevent rain and dew penetration into the welds, but having the upper surfaces painted presents a pleasing appearance. The photo in fig. 3 shows a freshly-painted tool drying before being rigged.

Figure 3. -- Freshly-Painted Tool Prior to Rigging

Each tool is rigged with a triangular chain tow bridle. It is towed from “chain towers” at the rear corners, with the “snout” out front providing both stability and ground clearance for the leading edge of the tool. A tow loop is “pinned” with a long bolt that fits any ball or pintle-hook type of hitch. There is a short length of chain through the “snout” braces that serves two functions: (1) an attitude-limiter on rough ground, and (2) the forward connection to the “snout” for using the tow bridle as a lift sling. The as-rigged chain bridle is depicted in fig. 4:

Figure 4. -- Tow Bridle Rigged and Extended Out Front

Fixed obstacles are to be avoided, since one is towing the tool on a steel chain, with essentially “no give”. If one hits a fixed obstacle, something somewhere will break, too fast for a human operator to respond. The intent is for the chain to be the “weakest link”, because a broken chain is easy to repair in the field, while the steel tool and the tractor hitch are difficult to repair. This action is analogous to the shear pin in a boat propeller mount.

This chain is a standard hardware-store item: either 3/16 inch or ¼ inch bar size proof coil chain is acceptable, smaller preferred, as long as the link dimensions can pass a standard 3/8-inch diameter bolt. The V-bridle piece is 16 feet, the short piece is 4 feet.

Each tool has a serial number and a manufacturer’s tag. Records are kept that indicate which tool went to each customer. These tags are located near the center of the ballast flat across the back of the tool. Between this ballast flat and the back end of the “snout” tube is the tool center of gravity. That is where one pins the bridle together with a single bolt, to create the lift sling. All of this is depicted in fig. 5:

Figure 5. -- Tags and Sling Lift Location Are Near Center-Rear

For short trips, the cactus tool can be carried in the bed of any half-ton (or larger) pickup truck. Just pick it up with the bridle in lift sling configuration, and set it down with the tailgate down. You will need two independent securing means to stay legal on the highways with a tailgate down. I use two small tow chains for this, as shown in fig. 6. Lashing it to a flat-bed trailer also works just fine.

Figure 6. -- Carrying the Tool in a Pickup Truck

Other Related Articles on this Site (date highlighted on this one)


Date.....…title/content
2-9-17....Time Lapse Proof It Works
............watch cactus being crushed and composted
7-30-15......New Cactus Tool Website
...................turnkey site for info,  photos,  videos,  purchases
1-8-15……Kactus Kicker Development
………………production prototype & 1st production article
1-8-14……Kactus Kicker: Recent Progress
…………..….testing a revised wheeled design (experimental)
10-12-13..Construction of the Tool
………………building a “Kactus Kicker” (plain tool)
5-19-13…….Loading Steel Safely
……………….transport and storage of materials
12-19-12…Using the Cactus Tool or Tools
……………...how the tool is employed (applies to any model)
11-1-12….About the Kactus Kicker
..…………….painting and rigging finished tools (plain tool)
12-28-11..Latest Production Version
………………new bigger snout and barge front (plain tool)