My wife got this for me off her Facebook. It is one of the better things I have seen. Enjoy.
Update 12-16-2021: This was just too good. We made our own. It's hanging in the entryway.
My wife got this for me off her Facebook. It is one of the better things I have seen. Enjoy.
Update 12-16-2021: This was just too good. We made our own. It's hanging in the entryway.
Update 7-15-2024: This article suddenly saw a brief spike of enormous readership in July of 2024! It became the all-time most-viewed-ever article here on this site, in only a few days! I saw no comments during that spike of readership, so I do not know who or why. But I hope those readers found it useful. THAT is why I post these things!
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Update 4-8-2024:
Should any readers want to learn how to do what I do (estimating
performance of launch rockets or other space vehicles), be aware that I have created a series of
short courses in how to go about these analyses, complete with effective tools for actually
carrying it out. These course materials are
available for free from a drop box that can be accessed from the Mars Society’s
“New Mars” forums, located at http://newmars.com/forums/, in the “Acheron labs” section, “interplanetary transportation” topic, and conversation thread titled “orbital
mechanics class traditional”. You may
have scroll down past all the “sticky notes”.
The first posting in that thread has a list of the classes
available, and these go far beyond just the
two-body elementary orbital mechanics of ellipses. There are the empirical corrections for
losses to be covered, approaches to use
for estimating entry descent and landing on bodies with atmospheres, and spreadsheet-based tools for estimating
the performance of rocket engines and rocket vehicles. The same thread has links to all the materials
in the drop box.
The New Mars forums would also welcome your
participation. Send an email to newmarsmember@gmail.com to find out
how to join up.
A lot of the same information from those short courses is
available scattered among the postings here.
There is a sort of “technical catalog” article that I try to main
current. It is titled “Lists of Some
Articles by Topic Area”, posted 21
October 2021. There are categories for
ramjet and closely-related,
aerothermodynamics and heat transfer,
rocket ballistics and rocket vehicle performance articles (of
specific interest here), asteroid
defense articles, space suits and
atmospheres articles, radiation hazard
articles, pulsejet articles, articles about ethanol and ethanol blends in
vehicles, automotive care articles, articles related to cactus eradication, and articles related to towed decoys. All of these are things that I really
did.
To access quickly any article on this site, use the blog archive tool on the left. All you need is the posting date and the
title. Click on the year, then click on the month, then click on the title if need be (such as if
multiple articles were posted that month).
Visit the catalog article and just jot down those you want to go see.
Within any article,
you can see the figures enlarged, by the expedient of just clicking on a
figure. You can scroll through all the
figures at greatest resolution in an article that way, although the figure numbers and titles are
lacking. There is an “X-out” top right
that takes you right back to the article itself.
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Update 10-29-2023: recently, I have received "comments" on this article that are nothing but ad solicitations from the makers of O-ring products, usually from overseas. They picked this article precisely because it mentions O-rings, which tells me this was the result of a keyword search of published articles on the internet. My blog site is not a monetized, commercial site. I do not accept any advertising from anyone. When I find them, I delete them.
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I have real difficulty with the fact that, even after all these years, it is still necessary to explain to people what really destroyed Space Shuttle Challenger and killed her crew, back in January 1986. It was really two very seriously-bad upper management decisions at NASA, one long before the launch:
(1) to insist on poorly-designing the O-ring seal joints with
3 interacting serious errors, and
(2) to fly soaked-out colder than had ever been tested, when everybody’s engineers did not want to.
Background
First, you have to
understand what really happens in federal government contracting. There is only one customer, and he thinks he is always right about
every decision that he makes. If you
do not do it exactly the way he wants, no
matter how wrong he might be, then
you lose the contract and you don’t get paid.
And, the government is
quite often wrong about how best to do things! That’s not to say the contractors are always
right, but they are wrong a lot less
often than the government.
You also have to understand that NASA never did know, and still does not know, the art of building reliable solid propellant
rockets. Essentially, no one at NASA ever did that kind of
work. They buy these things from
contractors who (by definition) know much more of the science, and especially the art, than anyone at NASA knows. The “science” is that knowledge which was written
down. The “art” is the knowledge that
was not written down, usually because
no one wanted to pay for the writing.
I can tell you from experience as an insider within the
business, that “rocket science”
isn’t really “science”! It is only about
40% science, about 50% art, and about 10% blind dumb luck. And that’s in production work! In new product development work, the art and luck percentages are even
higher.
Further, this same
sentiment applies to pretty much any type of engineering effort, not just rocket work. That explains a lot, about a lot of things, doesn’t it?
Poorly-Designed O-Ring Seal Joints
What I show in Figure 1 is how such joints should
be designed and built. This is the
design that most solid rocket motors use, very successfully, whether large or small. In most rocket motors, you need only join the aft and forward
closures to the case cylinder. Only in some
of the really large motors, the case
cylinder itself is divided into segments that must be joined, usually to limit the size of the case-bonded propellant
masses that must be cast and cured within them.
The sketch in the figure is what mechanical engineers call a
“radial static seal”. It is “radial”
because the O-ring lies between an inner and an outer surface, that must include a gap of tightly-controlled
size between the two parts, for
assembly. One part stabs into/inside the
other, in order to join them, in this case by a row of pins. It is “static”, because the parts, once joined,
do not move anymore. There are
strict but well-published guidelines and procedures for sizing the O-ring
groove dimensions, the gap for
assembly, and the size of the
O-ring, as well as its material
composition and its hardness. These
guidelines and procedures are used precisely because they work so very
well. Examples: Refs. 1 and 2.
Something also shown in the figure is peculiar to solid
rocket motors, especially those that are
segmented-case designs. There is a joint
in the insulation (and thus also the propellant) that leads to the sealing
surface gap, that in turn leads directly
to the O-ring in its groove. You DO
NOT obstruct this path with sealants,
putties, greases, or anything else! But there does need to be a
right-angle bend, to stop radiant heat transfer
from the flame in the motor from heating the O-ring directly.
The air in this path is what gets suddenly compressed upon
motor pressurization, and which in turn
forces the O-ring to the far side of its groove, where it gets squeezed against that surface
to seal. This is called “seating the
O-ring”, and until it is properly seated, it CANNOT seal, and so it briefly leaks!
Figure 1 – A Properly Designed O-Ring Seal Joint
It is the air in the path that gets compressed against the
O-ring, with hot booster gases and hot
solids filling most of the path volume that the air formerly occupied. But the air cools by convection to the steel
much more effectively and faster than to the O-ring itself. THAT is how the O-ring is not damaged by the hot
air, or the hot gases! The hot solids are stopped by the right-angle
bend. This is a rapid transient on a
time scale equal to, or shorter than, the motor pressurization event.
What you DO NOT want is contact of the hot gases (and
especially the hot solids) upon the O-ring!
The “hot sandblast” effect of that outcome would cut through the O-ring almost
instantaneously.
Note that these two design requirements of (1) one O-ring
and (2) an unobstructed pressurization path,
will interact very strongly with how one verifies proper assembly of the
motor! You must do a pressure
leak check of the motor to verify sealing,
but you must do it by pressurizing the entire motor! However, you NEED NOT pressurize the motor to its
full operating pressure to do this verification!
You only need an atmosphere or so of pressure difference to
seat any O-ring and then verify its sealing.
If it holds at that low pressure,
and you followed the design guidelines correctly, it will hold at full motor operating pressure! THAT is what you verify when you
do motor case hydroburst testing, long
before you ever cast propellant to make a live motor! That’s the way the real solid rocket motor
manufacturers prefer to do it. And it
works to very high reliability levels,
as indicated in the figure.
However, that is
NOT what NASA insisted upon doing!
In the mistaken belief that a second back-up O-ring increases
sealing reliability, they insisted upon
the two O-ring design indicated in Figure 2. Thiokol complied, lest they lose the contract. In the mistaken belief that they had
to pressure leak check at full motor operating pressure, NASA did not want to risk fully pressurizing
a live loaded motor (and rightly so). And
so NASA insisted on a way to apply air pressure at full motor operating
pressure, between each pair of
O-rings at every joint, instead of any motor
pressurization. This is shown in the
figure.
What this does is drive the downstream (backup) O-ring to
the correct side of the groove, thus
seating it for motor operation.
But, it also drives the
upstream (primary) O-ring to the wrong side of its groove, from which motor pressurization upon ignition
must unseat it, drive it across its
groove, and re-seat it on the correct
side! Until and unless it re-seats on
that correct side, the upstream
(primary) seal ALWAYS leaks!
Period! There is NO WAY AROUND
that outcome! And THAT lets hot
gases and solids reach the primary O-ring,
simply because the re-seating process takes a longer time than
pressurization!
Figure 2 – The Improperly-Designed 2 O-ring Joint That
Flew, Up Through Challenger
NASA made a third mistake: in the mistaken belief that it
would prevent hot gases and hot solids from reaching the O-ring, they insisted on obstructing the
pressurization path by filling the insulation joint with “heat protective”
putty (zinc chromate putty actually).
This is also shown in the figure.
This last mistake makes a bad risk even far worse, because high pressure gases always
(ALWAYS!!!) “wormhole-through” a not-solid material (like putty or grease) at a
single point! THIS effect is also shown
in the figure. That re-distributes the
“push” of the gas from a broad front all around the O-ring, to a single point upon the O-ring, as indicated in the figure. The delay unseating the ring, pushing it to the other side of the
groove, and reseating it, almost guarantees that the compressed air
leaks past it, so that booster hot gases
and solids can reach the O-ring. And
those will cut a hole right through it.
“Half-moon slices” right through the primary upstream O-ring were seen, upon SRB motor disassembly, in a rather significant percentage of the SRB’s recovered and refurbished. That verifies what I just said about the upstream O-ring being cut! There is no surprise there, once you understand the process!
The difference between this point load problem, and what NASA analyzed in its structural
calculations for the O-ring seal is quite stark! The structural analysts were assuming
pressurization on a broad front. They
did not model the point load effect of the hot gases and solids
wormholing-through the putty obstructing the pressurization path. Quite simply, what was built was NOT what was analyzed!
Unnecessary Risk to Fly Too Cold
If the motor is sufficiently cold-soaked, the primary upstream O-ring loses its flexibility
and resilience (as do all of them).
Pushing the entire embrittled O-ring across its groove all at once is
risky enough, but if you concentrate the
“push” at one single location by the wormhole effect, you essentially guarantee snapping the
O-ring apart at that point! This
cold brittleness effect was amply demonstrated by Dr. Feynman at the Rogers
Commission hearings (assisted by Gen. Kutyna),
when he stirred his sample of the O-ring material in his glass of ice
water, and then demonstrated its non-resilience.
Any failure of the primary upstream O-ring, whether by hot sandblast cutting, or by cold brittle fracture from the point
jet force load, then puts a single-point
hot sandblast jet impacting onto the downstream O-ring, simply because it is nearby! Thus, a sort of “cascade failure” is a very high
risk indeed!
The post-Challenger “fix” was a third O-ring in every
joint. This just set up the cascade
failure as a longer chain, as indicated
in Figure 3. The only
reason the Challenger disaster did not repeat is that they never flew that cold
again. But the 1/51 failure rate
demonstrated by loss of Challenger speaks for itself!
Figure 3 – The Cascade Failure Risk Was Compounded By the
Redesigned Joint
Fatal Consequences We All Saw
The photography obtained during the launch and loss of
Challenger confirms everything claimed here.
The seal failed upon motor ignition and pressurization, as shown quite clearly in Figure 4. The dark grey plume is carbon soot-bearing
hot gases spewing through the two failed O-rings at the aft segment joint.
Figure 4 – Seal Leak Upon Ignition Seen In Photography
This leak miraculously “cured” itself by plugging-up with
aluminum oxide-carbon slag from the metallized propellant. This slag-plugging just happened to hold
pressure like that, until the Challenger
encountered a wind shear while at “max-Q”, where it was also most highly stressed by
aerodynamic forces. The slag plug
failed, letting the hot motor gases and
solids rush through the hole again. This
is shown quite clearly as the anomalous bright-but-small extra plume in Figure
5 below.
This jet of leaking hot gases and solids finally got so big that
it cut through one of the aft struts holding the SRB to the center tank. There is always hydrogen leaking from the
center tank’s hydrogen tank, and in
this case the leaked plume probably burned a hole in that hydrogen tank. With the strut cut, the bottom of the SRB moved outboard. That pushed the nose of the SRB inboard, such that the nose of the SRB poked a hole in
the side of the center tank’s oxygen tank.
Suddenly dumping oxygen into a base-burning hydrogen-air
fire caused an explosion in the wake behind the center tank that both
overheated and structurally overloaded it.
The tank collapsed, letting both
SRB’s and the orbiter fly free. The
released propellants burned explosively as this happened. All this happened in an instant, so it looks like just the one sudden explosion.
Figure 5 – Leakage Resumed After Being Shaken By Wind
Shear at Max Q
The released SRB’s continued to “fly” out-of-control under
their own thrusts, as we all saw. This is shown in Figure 6. The orbiter’s engines were pointed through a
center of gravity that suddenly no longer existed, so they forced the orbiter to pitch-up
violently, before starving for lack of
propellant from the suddenly-missing center tank. The pitched-up orbiter went broadside to the
supersonic wind, which tore it to
pieces. This is how those pieces, that we all saw fall into the sea, came to be.
Figure 6 – The SRB Did Not Explode, But It Punched a Hole In the Center Tank
Final Remarks
The two O-ring joint was a NASA-mandated design
mistake, compounded by mandating putty
obstructing the O-ring pressurization paths.
The “customer is always right” in government contracting, except that he was lethally and fatally
wrong about this one! See
also Ref. 3.
The decision to fly cold-soaked colder than the SRB’s had
ever been tested, was also a NASA management
decision. Both NASA and Thiokol
engineers objected, but were
over-ruled. Thiokol upper management
also over-ruled their own engineers, and
told NASA to go ahead and launch. Thus
emboldened by Thiokol management, NASA
launched the thing, thus killing its
crew.
The stand-down to “correct” this problem was nearly 2 years
long and horribly expensive. Which just
goes to prove what I like to say to anyone who will listen: “there is nothing as expensive as a
dead crew, especially one dead from a
bad management decision”.
The only problem with that return-to-flight effort is that they
did not correct the real problems upon return-to-flight, they actually made them worse with a 3-O-ring
joint, and by keeping the putty
obstructions. The ONLY thing they did “right”
was never to fly that cold again!
Which is very likely the ONLY reason that the Challenger disaster did
not repeat itself before the Shuttle got retired, since there were more than 51 more flights
after the Challenger disaster!
By the way, the crew
did not die in the tank explosion and subsequent ripping-apart of the
orbiter by air loads. The telemetry
showed no high-gee accelerations at all!
The crew was still alive in the orbiter cabin until it finally hit the
sea, which is about a 200-gee stop, since it hit dead broadside. See Figure 7.
Figure 7 – The Crew Was Still Alive In This Cabin Section
(Arrow) That Is Falling Back
I say what I said about the crew because the flight deck
back-seaters leaned forward and flipped on the breathing-air packs for the
front-seater pilots. They would not have
done that unless they knew the cabin had depressurized, and that would have been significantly
AFTER the explosion and ripping-apart of the orbiter. They were tumbling clear of the explosion
cloud by that time, as illustrated in
the figure.
Those two flight deck pilots had breathed-up all the oxygen
in their breathing packs by the time they hit the sea, something confirmed by the empty breathing
packs that were recovered. Which
means they were alive when they hit the sea! By extension,
so were the back-seaters, plus
the three down on the mid-deck.
They did not have pressure suits, parachutes,
breathing bottles, and a hatch
they could blow open (basic bail-out gear).
More importantly, there was
no way to take the spin off the tumbling cabin. Spinning like that, there was no way to reach and exit the
hatch, even if they had the other basic
bailout gear! But a small
drogue parachute from the nose of the cabin section would have taken off the
spin! That plus the basic
bail-out gear just listed could have saved that crew! It took almost 5 minutes to hit the sea. They had the time to bail out.
I submitted that means for bail-out to NASA, but I was ignored. Coming from an outsider, my idea was “not invented here”, as far as NASA was concerned. Yet, something
rather like it might even have worked for Columbia some years later: the 3 mid-deck occupants were still alive inside
a tumbling cabin section as it approached impact near Tyler, Texas, well after the breakup during re-entry. Time was short for a bail-out, but without the de-spin drogue, they could not reach the hatch at all.
References
#1. Parker O-ring Handbook ORD 5700, copyright 2021, original release 1957, Parker O-Ring and Engineered Seals
Division, Lexington, KY, available from parkerorings.com
#2. Seal Design Guide,
Apple Rubber Products, Lancaster
NY, available from AppleRubber.com
#3. Wikipedia article “Rogers Commission Report”, in this case accessed 11-26-2021
Final Notes
There are different design rules for static radial and
static face seals, and different rules
yet for dynamic radial seals (as on a piston moving inside a cylinder, like a syringe or a hydraulic cylinder). The Shuttle SRB joints fall into the static
radial classification.
The appropriate set of rules specifies O-ring sizes and
hardness, groove dimensions, and when to use back-up rings. You just follow the design rules, and make sure that only compressed air
reaches the O-ring (and on a broad front),
upon solid propellant motor ignition.
You accomplish that broad-front pressurization with the
90-degree bend geometry to stop the hot solids and radiant heat transfer, and by NEVER obstructing the O-ring pressurization
path with anything! Even too close a fit
between the hard parts, can cause
problems with the transient pressurizing flow.
You verify your seal design,
your case structural design, and
your leak check procedure, during
case hydroburst testing, long before
you ever cast a live motor! You
NEVER delete the hydroburst testing step in your development effort. Never!
Not for any reason at all!
Then you test live motors at every environmental extreme
condition in which you think you might possibly operate. If any redesigns (of anything) are
needed, you go back and verify them in all
the tests, from hydroburst all the way
forward. No motor goes to production, until its exact design configuration
has been verified in every test at every test condition!
Once your design has passed all those tests, you stick with your verified leak check
procedure as if it were a religious mandate!
You add rigorous quality control (of the “total quality management”
type), for production. That includes X-raying every single item, to verify that there are no casting voids in
the propellant, no unbonds between
propellant and case liner, and no other propellant
grain cracks or other problems. And then
you NEVER operate a motor outside the conditions for which it was tested!
THAT is the way to achieve no-more-than-1-in-a-million
failure rates, with solid propellant
rocket motors!
The “bean counters” and “management professionals” will
absolutely hate that prescription as “too expensive”, but killing a crew with a bad design just costs
a whole lot more, than the cost of
following that prescription. We’ve
already seen that with Apollo-1,
Challenger, and Columbia.
Simple as that.
And just as hard to sell to the “bean counters” and
“management professionals”, as you might
fear.
One of the most unusual ramjet projects I ever worked on was a non-propulsive device. This was a very miniature ram-fed airbreathing combustor, that was to be the hot gas generator for an infrared (IR) decoy. This decoy was to be towed behind an aircraft in lieu of a whole series of dispensed flares. It was intended to work by having enough IR output to cause the aircraft to drop out of the missile field-of-view first. See Figure 1 for that concept. I was working for my friend Byron Hinderer doing this.
Figure 1 – Towed IR
Decoy Concept, called “Warm Brick” at
Tracor in 1984
I did this at what was then Tracor Aerospace, in Austin,
Texas, during 1984. We called this decoy “Warm Brick”, and my job was to determine if this concept
was even feasible (it was). Our idea was to
heat a porous refractory material until it glowed brightly in the IR. We preferred fuel-air combustion to minimize
decoy mass, and ram combustion is the
simplest of the airbreathers. Plus, I had lots of experience with ramjet
combustion at what was then Rocketdyne/Hercules in McGregor, Texas.
To the very best of my knowledge, no patent was ever taken out on this
concept, and Tracor never did anything
at all with it. Even if there had been a
patent, and it had been
renewed, any such patent would have
run out by now. So, what I reveal here should offend no one, and infringe no patents.
As implemented for the feasibility tests, this concept took the form of a “gasoline
lantern mantle” made out of commercial ceramic fire curtain cloth, as the IR emitter. This was to be mounted behind a wake-producing
spoiler, mounted at the aft end of the
burner and inlet assembly. The decoy
might carry its own fuel tank, or it receive
fuel down its tow line, if a heavier tow
line could be tolerated.
To test the scientific and engineering feasibility, I designed a very generalized inlet and
burner hardware set that was flexible enough to allow evaluation with a variety
of gaseous and liquid fuels. See
Figures 2 and 3. The intended
flight conditions were relatively low altitude from mild subsonic to
barely-supersonic speeds, typical of an
attack aircraft threatened by surface-to-air missiles.
Figure 2 – Assembly
Sketch for the Initial Version “Warm Brick” Ram Combustor Test Device
The assembly sketch clearly depicts the long fuel
injection-and-mixing duct allowed between the inlet diffuser and the sudden
dump into the combustor. There was an
inlet piece and a fuel injector piece,
both made of aluminum for ease of rework, and an inlet tube and a combustor shell, both made of steel. The combustor shell was sized for fabrication
from 2-inch schedule-40 pipe, but ended
up being made of 300-series stainless to those same dimensions. We tried automotive-style spark ignition.
One can easily see how the molded low-density ceramic liner
insert was to be trapped in place by the nozzle block. The arrangement shown in the assembly sketch of
Figure 2 (directly-pinned nozzle block) was quickly replaced by a pinned steel
nozzle shell ring, as shown in the
hardware photo (Figure 3). This revision
happened about the same time that the first (unreinforced) liner was replaced
with the second liner (reinforced ceramic composite).
Figure 3 – Photo of
the “Warm Brick” Ram Combustor Test Hardware as Revised
The design concept called for a small combustor fed by a
simple pitot inlet, with a convergent-only
nozzle that would likely function unchoked at most conditions. I chose a center-duct coaxial air entry with
sudden-dump flame stabilization, similar
to the successfully-flown ASALM-PTV liquid-fueled ramjet test vehicle. Geometric
ratios were initially set equal to those used in ASALM.
Based on Reference 1, I chose a minimum ¼-inch (6 mm) step height
around the dump. The combustor length
was sized “empirically” (rules of thumb based on ASALM-PTV geometry) so that
the annular separation bubbles would close,
and the axial core would be “burned out”, before any of these flows entered the nozzle. That was basically an assumed 11-degree
spreading angle, on both sides of the
mixing layer between the entering mixture and the recirculated flame. That’s
too crude, in hindsight.
We wanted sufficient porosity in the emitter so that the
burner operation would be unaffected by the presence or absence of the emitter. The fire curtain cloth gave us that, in the sizes tested, because the surface area of the ellipsoidal
shape was so large relative to the final burner throat area. Its effective porosity-driven “free” open
area was very much larger than any of the burner throat areas we tested.
There were two crucial unanswered questions: (1) emitter/hot gas coupling (could we
really get the emitter hot enough to radiate effectively?), and (2) obtaining stable combustion at all
in a burner that small, with any fuel
whatsoever! There was an extensive paper
trade study done, to determine the desired
fuels. In test, these fuels,
and some other fuels that were easier to use, were investigated.
This combustor was nominally 1.5 inch (38 mm) inside
diameter, as insulated, and 3 inches (76 mm) long inside. The smallest size ramjet combustor in my
experience up to that point had been some heavyweight solid-propellant ducted
rocket ramjet work (in a completely-different geometry) at 4.6 inch (117 mm)
inside diameter, and length/diameter
6-to-8. The largest was ASALM-PTV at a
20 inch (51 cm) combustor case diameter.
“Warm Brick” was smaller than anything of which I had any knowledge!
I didn’t want to periodically replace an ablative liner in
the test burner, and I didn’t want to
attempt an air-cooled liner shell for full-rich combustion in something that
small. So I opted for an unknown, inspired by the Space Shuttle’s heat shield tiles. Could I put a low-density ceramic insulator
in this combustor, and not melt it? The answer turned out to be “yes”, but it took some adaptive effort.
The project operated in three logical parts: (1) obtain stable combustion with a variety
of fuels in the burner alone, (2) add
the emitter and determine how best to shape,
fabricate, and attach it, and (3) document infrared radiometric
output. The real prerequisite for part
(1) was the combustor insulator, since
we started with gaseous fuels, thereby
avoiding the fuel vaporization issue.
I selected free-jet test mode as the best way to accomplish all three parts of
this project with the same hardware and test setup (see
Figure 4). All that I had
personally done while at Rocketdyne/Hercules was direct-connect testing, but I knew about free-jet testing, both from my research, and some experimental association with
Marquardt, while I was with
Rocketdyne/Hercules.
We used a commercially-rented air compressor trailer as our
air source, to be run real-time. In 1984,
this 750 SCFM unit was the largest of its kind in Texas. It fed a PVC pipe stilling chamber, terminating in a simple convergent-only
nozzle block made (conveniently) of wood.
Figure 4 – Test
Setup: Stilling Chamber Exhausting To Left, Fed From Right
The test article was bolted to a heavy pipe
stand-and-sting, with its inlet immersed
in the free jet of air. That free jet
typically measured 190 F (88 C) stagnation temperature, at full-power compression conditions.
The first part of the investigation began with bottled
hydrogen gas fuel (series 1). This and
all the other trials are summarized in Table 1 below. Series 1 wasn’t very successful for two
reasons: (1) the nozzle was too wide
open for a stable flame, and (2) free
jet air speeds higher than about 0.25 Mach blew the spark column out from the
electrodes of the spark plug, even
though it was located flush within the annular recirculation zone.
The device didn’t ignite at all until I obstructed the
nozzle with a scrap of wood, and it still
went out after ignition, if I removed
the obstruction. So, I built a smaller-throat nozzle block. We still had to ignite at low airspeed and gradually
work up to higher speeds, limited at
that time to about half a Mach number by the stilling chamber nozzle. I also tried liquid ethanol unsuccessfully at
this time (series 2).
Somewhere in all of this,
I first drove the combustor into what proved to be a very
violent rich blowout instability,
and completely shattered my first (unreinforced) liner! The combustor visibly shook on its
sting, and it spit the pieces of its
liner out the nozzle, igniting a local
grass fire! Later, we estimated a pressure amplitude near 0.8
atm, at audio frequencies (a few hundred
Hertz), for this instability.
A photo of the liner molding tools that I used is given
in Figure 5, which includes the
basic combustor shell as the outer forming tool for the combustor liner. Both it and the nozzle block were laid up as
(commercial) low-density molding compound troweled onto the wooden plug, and inserted into the corresponding shell for
cure. I used Cotronics Corp. 360M low-density
molding compound for this.
Figure 5 – Tools Used
for Molding Ceramic Combustor Insulation Liner Inserts
These parts were cured at 215 F (102 C) in an oven to drive
off the water. The circuitous paths for
exiting steam led to a low density ceramic matrix. The resulting parts were coated with a
paint-like ceramic cement (Cotronics Corp. 901), and cured again, in the same oven. The unreinforced liner showed evidence of hot
gas flow behind the insulation, and into
the cracks, shown in Figures 6 and
7.
Figure 6 – Recovered
Pieces of Shattered Unreinforced Liner,
Bonded Together
Figure 7 – View of
Fracture Surface, Showing Hot Gas Flow
Damage with Sooting
I built a second ceramic composite liner reinforced
by layers of the fire curtain cloth (woven from 3M Nextel 312), which survived all instabilities and any
other test abuses thereafter. It
survived many hours of accumulated burn time in near-pristine condition, as seen in Figures 8 and 9. The shrinkage cracks did not preclude
functionality. There was some melting evident
in the throat of the nozzle.
Figure 8 – View Into
Near-Pristine Reinforced Liner, After
Hours of Burn Time
Figure 9 – View Into
Reinforced Nozzle Block, After Hours of
Burn Time
Once we had the burner working at all, we tried some test sample pyrometers in its
exhaust plume, with both propane and
acetone as fuel (series 3, and acetone
proved worthless as a fuel). These pyrometers
would be old nails, or else planar
samples of potential emitter materials.
We even tried gasoline as fuel (series 4), but results were poor, and it became very obvious that poor
vaporization was the cause! I tried propane
again (series 5) as the most successful fuel,
and got enough radiometer output to be encouraging, from a sample of the fire curtain cloth
immersed in the jet exhaust.
So, I created a
fuel-line hot-soak bucket to correct the poor fuel vaporization problem for
test purposes. This took the form of an
electrically-heated bucket of old motor oil,
in which a coil of the fuel supply line was immersed. That rig is shown in Figure 10. It may resemble a moonshine
still, but it is not!
Figure 10 – Fuel
Vaporization Preheat Bucket Rig
At this point, I had
a crudely-successful burner, but an
unproven fuel supply method. I checked
out the combined burner and fuel vaporization bucket, first on propane (series 6), then on aviation gasoline (series 7), and finally on a “home-made version of JP-4” that was actually half Jet-A and half
aviation gasoline (series 8). Plus, I added instrumentation to the burner unit
(enough manometer pressures and thermocouples to attempt an actual “engine” cycle
analysis).
Results, including the
exhaust pyrometer samples, were
favorable enough to warrant continuing the project further. It still required a lower-airspeed
ignition. I stood in the jet blast for
all these tests, looking directly into
the flame zone, and sniffing for unburned
fuel, to set mixture. That “settled” the fuel injection and
ignition issues well enough to test emitter coupling issues for the very first
time.
The first actual emitter was made of Nextel 312 fire curtain
cloth, coated with the Cotronics 901 adhesive
as a “paint”. It was sewn together, with alumino-silicate thread, from bias-cut gores much like a balloon, to form an elongated semi-ellipse
approximation. The seams were left on
the outside of this first emitter, as
shown in Figure 11. It was the
first of several series 9 tests with pre-heated propane, at air speeds up to about Mach 0.47. Those test conditions are depicted in
Figure 12.
Figure 11 – Test
Setup for First-Article Emitter
For all subsequent tests,
the seams in the sewn emitters were placed to the inside, as is depicted in Figure 13. That photo shows post-burn appearance of two
series 12 emitters tested with ethanol fuel,
but all the internal-seam emitters appeared similar, regardless of series and fuel.
These articles were brittle and fragile post-test, as expected for alumino-silicate materials
soaked to temperatures exceeding the solid phase-change temperature of about
2350 F (1290 C). That fragility alone
confirmed a high surface temperature for radiation purposes! This was also verified by radiometric
measurement, which also indicated very “non-gray”
behavior, in that the effective color
temperature (radiation peak wavelength) was substantially cooler than the
actual temperature.
The spoiler just ahead of the emitter clamp mounting
provided protection from direct wind blast forces. Plus,
it also provided effective hot gas recirculation effects external to the
emitter surface. Both acted to raise
emitter material soak temperature, and
therefore IR output, quite successfully.
Figure 12 – Test
Conditions Explored with Series 9 Propane
Two tests were made as series 10 in this same configuration
with the “home-made JP-4” fuel. Results
were similar to the series 9 propane runs,
except for a small liquid-wet “cold spot” at the very end of the emitter
bulb. This was due to still-unvaporized
kerosene hitting the emitter on-axis.
Figure 13 – Post-Test
Emitter Appearance from Series 12 Ethanol Tests
Sometime during this checkout process before the series 9
propane runs, I successfully modified
the inlet to a larger lip radius, in order to decrease its “buzz” instability
tendencies at higher backpressures. That
also greatly improved ignition characteristics,
and it further pushed the rich blow-out instability limits to richer
mixtures! The test set-up for cold-flow
inlet calibration is shown in Figure 14.
Both the original and modified (larger lip radius) inlets
were cold-flow tested with this rig.
Data were cross-plotted in a variety of ways. The data plot format for “typical” supersonic
ramjets was rather undiscriminating at these subsonic speeds: stream tube area ratio versus Mach and
stagnation pressure recovery ratio versus Mach.
Plots in the more primitive-variable format were actually more useful
for this mostly-subsonic system. These
included the diffused Mach to freestream Mach ratio, and the static “pressure gain” ratio.
These results guided the 1984-vintage data reductions of the
series 9 propane runs with emitters.
From those, installed hot-burn
test inlet performance data matched the cold-flow tests. The streamtube area recovery ratio shows a
very strong influence of the so-called “highlight” area versus the true minimum
area, when used as the reference area for
the calculation.
After the fact, this was
entirely expected, based on Reference
2, which (of course) recommends
the highlight definition. At the time I
did these tests, I had used something
pretty close to the minimum area for the reference. It
shows explicitly in the data, as a
recovery ratio substantially greater than unity, which is completely out-of-line with the
usual expectations for ramjet inlets.
See Figures 15 and 16.
Figure 14 – Cold-Flow
Inlet Calibration Test Rig
After the series 9 and 10 tests, the air nozzle in the stilling chamber was
replaced with a second wooden unit of slightly smaller throat diameter, as depicted in Figure 17. This enabled free jets of nearly Mach 1 speed
at the maximum compressor output. Two
more test series were conducted with this change, specifically to obtain data at those higher
simulated air speeds. These were series
11, using both propane and hydrogen
fuels, and series 12, which used the finally-selected ethanol
fuel.
The series 12 tests employed both radiometer
measurements, and imaging with a thermal
imager camera. The fuel vaporizer rig
was less successful with a high latent heat pure-substance fuel (ethanol), than it had been with distillate fuels, or with the easily-vaporized propane. With ethanol,
it was essentially long-period unstable,
with an oscillating fuel flow output.
The cycling time was a few seconds.
Nevertheless, using
ethanol fuel produced an output spectral power distribution closer to what is
needed from the non-gray decoy. The radiometer
data clearly showed this. We attributed
this difference (with a high degree of confidence) to the lack of yellow carbon
glare in the ethanol flame. This yellow
carbon glare was quite noticeable in the propane tests, and even more so when using gasoline or jet
fuel. The series 12 ethanol runs looked to
the eye “positively white” in comparison.
The ethanol fuel injector was stopwatch-and-bucket
calibrated for those series 12 tests. Those calibration data are shown in
Figure 18.
Figure 15 –
Calibrated Inlet Performance Derived from Series 9 Data, Part 1
Figure 16 --
Calibrated Inlet Performance Derived from Series 9 Data, Part 2
Figure 17 – Air
Nozzle Re-Work for Higher-Airspeed Test Capability
Figure 18 – Flow
Calibration Data for the Series 12 Ethanol Fuel Runs
After these tests,
the fuel vaporization problem was conceptually addressed as a hot-gas
tap from the forward end of the combustor to the lower-pressure zone at the
minimum area of the inlet. Fuel would be
injected into this very hot recirculated gas stream to effect rapid
vaporization. While the design analysis
looked good, that concept never
received any testing due to budgetary constraints that essentially
stopped all experimental work on the project after late 1984. Some prototype flyable hardware was
designed, and a few of those parts
manufactured, before all work on the
project was completely stopped. It
never resumed. So NOTHING is
confirmed about any of this!
The ceramic liner material was never characterized, it “just worked”. Density,
strength, and thermal conductivity
were never measured in any way!
However, it handled as if it were
about as dense as commercial Styrofoam products. The strength was considerable, considering the rich blow-out instability
abuse it endured. Immersed in a 190 F
(88 C) air stream, the combustor shell
would “barely boil spit” after an hour-long burn test at full rich mixture
(theoretically around 3800 F or 2100 C),
with but 0.2 inch (5 mm) thickness of the insulation! That indicated very low thermal conductivity
indeed!
Table 1 – Summary of
“Warm Brick” Burner Tests
These recent compressible-flow cycle analysis results
defined the bulk flow conditions inside the combustor well enough to attempt a
heat transfer model with a reasonable expectation of success. That model was cylindrical convective-conductive, and based on standard compressible flow
models inside and outside the combustor shell.
Radiative loss was near zero, as
there was no effective path by which thermal radiation could leave the
interior. The shell radiation cooling potential
was very low.
While the steel shell has a well-known thermal conductivity, the ceramic composite liner did not, so I ran this model parametrically versus
conductivity values from “very low” to “very high”. The “best” value of thermal conductivity was
that which matched both my recollections of perceived shell temperature, and my observation that the liner
surface was often close to melting (3250 F, 1790 C).
Those thermal conductivity results are given in Figures
21 and 22. The highlighted value
of 0.02 BTU/hr-ft-F equates to 0.035 W/m-C.
Density and strength still lack actual characterization! I have often wondered whether this material
might serve as a re-entry heat shield material, the way that the somewhat-similar low-density
ceramic Shuttle tile did. But that is
another topic for another venue.
References:
#1. Curran, Edward
T., “An Investigation Of Flame Stability
In A Coaxial Dump Combustor” (dissertation,
AFAPL/RJ WPAFB, Dayton, OH),
AFIT/AE/DS 79-1, Jan. 1979.
#2. Seddon, J., and Goldsmith, E. L.,
“Intake Aerodynamics”, AIAA
Education Series, 1985, ISBN 0-930403-03-7.
Figure 19 –
Spreadsheet Setup for “Warm Brick” Cycle Analysis at Series 9 Propane
Conditions
Figure 20 –
Spreadsheet Cycle Analysis Results for “Warm Brick” at Series 9 Propane
Conditions
Figure 21 – Heat
Transfer Model Results for “Warm Brick” Liner Thermal Conductivity
Figure 22 – Heat
Transfer Model Results Plotted vs Radius
Epilogue: Some Practical Combustion Device Lessons
Learned
Cycle analysis with one-dimensional flow models turned out
to be less important than the actual scale-dependent physical chemistry of
flame stability, for this “Warm
Brick” device. Residence time is proportional to dimension, all else equal, while chemical reaction rates are
scale-independent. This alone suggests
there is a minimum size below which a thing “just won’t work” with a particular
fuel.
Mixing is another very strong determinant of flame
stability. Mixing is not proportional to
scale, nor is it scale-independent, but it is something in-between. Again,
this also suggests that there is a size below which a thing “just won’t
work” with any particular fuel. That is
precisely one issue (of many) in flameholding.
Those considerations explain why the required nozzle
contraction ratio (and internal flow velocities) were so low in the “Warm
Brick” device for stable ignition and burning,
relative to everything I knew about, before I attempted this project. However,
these experiences with the Warm Brick subminiature combustor predate the
in-depth understanding of flameholding and flame stability that I was later
able to achieve, after returning to
Rocketdyne/Hercules. That knowledge is
summarized in the “exrocketman” article titled “Ramjet Flameholding” (on this
site) and dated 3 March 2020.
The vaporization of fuels of different latent heats and
boiling behavior revealed a surge instability in the hot-bucket fuel rig
(referring again to the crude hardware in Fig. 10 above). The basic layout was a source of fuel at
pressure, led through a copper line
coiled in the hot bucket, and from there
to the metering orifices inside the test article. See the cartoon in Fig. 23.
The source of fuel-at-pressure was a standard 5-gallon
propane bottle (usually around 200-250 psig),
or a welding gas bottle (initially 2200 psig), or a pressure tank of liquid fuel pressurized
with compressed dry nitrogen (usually pressurized in the 100-300 psig range). All of these pressurization schemes are
regulator-controlled. That regulator was
physically located about 5-to-10 feet downstream of the test article, and within arm’s reach of the exhaust
plume. This allowed me to manually
adjust the fuel flow during the test by varying the regulated pressures, while standing immersed in the exhaust where
I could smell for unburned fuel. For the
open-nozzle tests, I could literally see
the flame up the tailpipe.
Fig. 23 – Conceptual Layout and Operation of Fuel Supply
When using hydrogen directly from the welding gas
bottle, there was no vaporization
problem, as this was simply compressed
hydrogen gas. We did not use a
pre-heater bucket with this fuel, but
the rest of the component layout in Fig. 22 is correct.
With propane in the 0.47 Mach air tests, we found the line just downstream of the
regulator, and the sides of the propane
bottle, to be cold. This is because the vaporizing pool of liquid
propane in the bottle must draw about 150 BTU/lbm of latent heat from itself
and from its surroundings, mostly
from itself (gets cold). If it
cannot draw sufficient heat to vaporize,
then it won’t vaporize, pressure
drop notwithstanding! The energy to
change phase (latent heat) simply must come from somewhere!
There was a cold-line risk of re-condensation on the way to
the test article, which we “cured” with
the hot oil bucket preheater. We kept
the line length from bottle to preheater as short as practical. We also found bottle “freeze-up” occurred at
the higher flow rates with the Mach 0.9 airstream tests. We “cured” that by the camper’s expedient of
putting the propane bottle in a tub of hot water.
With gasoline and jet fuel,
the driving pressures helped us pre-heat the liquid fuel without getting
any boiling in the fuel line. Without
preheat, there was insufficient air
stream heat in the test article to get the fuel to vaporize and burn. With about 300 F preheat, we got all but the “tag-end” of the
distillation curve to vaporize upon being injected, due to combined atomization and pressure-drop
boiling.
With the gasoline and 300 F preheat, our nominal 100-300 psig driving pressure was
apparently barely enough to prevent any significant boiling in the line, so we did not encounter any noticeable problems
with vapor lock-induced fuel flow rate surges.
With the jet fuel and its lower volatility, we had no real risk of vapor lock
surging, but we did see a little more
“tag end” unvaporized fuel, indicating a
higher preheat temperature was really needed.
Both of these are about 150 BTU/lbm latent heat materials.
We did have a real fuel surge problem running neat
ethanol as fuel. This material has a
far higher latent heat at about 378 BTU/lbm,
and it has a single normal boiling point, instead of distillation behavior. At our delivery conditions, the pressure was insufficient to prevent
boiling in the line, leading directly to
vapor lock-induced flow rate surging!
Fuel delivery rates oscillated through about a factor of two, on a long period of several seconds. It would vapor lock, unlock,
and relock to cause this surging.
We could not reduce preheat temperatures and still expect to
get any flash vaporization upon injection,
in hindsight due to that higher latent heat. We could not increase the feed pressures to
preclude the boiling without re-working the test article for much smaller
injection orifices. That latter is the real
design solution to this problem, but we
did not use it for these tests! We were
able to get our infrared radiometer data from the high points of the
oscillating-intensity burn.
While high pressure preheat to get flash vaporization from
an atomizing injector is an approach that really works, the equipment to do it is usually large and
heavy, too much so for a miniature decoy. The alternative would be to mix the fuel with
hot combustion gas to get vaporization,
downstream of the metering point.
The design difficulty is then to get good mixing of the fuel-rich gas stream
with the inlet airstream, without
suffering large pressure losses. That
seemed the better approach for the flight decoy design. We were never able to test this, though!
It is still just a concept!
For an aero-engine application, high-pressure fuel pre-heat with atomizing
flash vaporization is likely the better design approach. The sizing of required preheat depends upon raising
the liquid to a temperature such that the enthalpy drop across the injection
orifice exceeds the latent heat of vaporization. The size of the orifice and the feed line
pressure determine flow rate. But, the feed line pressures must always exceed
fuel vapor pressure at that high preheat temperature! If this is not done, then vapor lock-induced surging will occur, and at very significant magnitudes. Fuel control then becomes impossible.
As indicated, we
never got to test the concept of vaporization by injection into a hot combustion
gas stream, followed by injecting that
hot mixed stream into inlet air. There
is a lot of promise in that notion, but
it is fraught with practical difficulties,
as well.
Final Comments: IR
Emission Characteristics and Towed Decoy Physics
The IR emission characteristics topic has been
mostly ignored here, except to say these
ceramics were decidedly “non-gray” in their spectrally-dependent emissivity
properties. They were non-gray enough to
reduce expected radiation in the 1-2 micron band very markedly, to near what they emitted in the 3-5 micron
band, despite operating at a temperature
somewhere near 3000 F (1650 C). The effective
“color temperature” (really the wavelength at peak spectral distribution of
radiation) was much closer to typical tailpipe temperatures at full power (but less
than those with full afterburning).
Suffice it to say that a great deal of infrared power was
radiated by a very small object, whose
color temperature and radiated-power in-band looked like a very large jet
engine tailpipe at full power. This
little emitter would blister my face with radiated heat from some 20 feet
away. The large radiated power would be
the temperature-to-fourth-power effect,
while the color temperature would be the non-gray emissivity
effect. Both are critical effects.
Exploring this IR emission topic in more detail would be the
subject of some future article, or
perhaps even a book relating these experiences.
This is an application of otherwise well-established physics.
Another unaddressed topic is aeromechanical in nature: how
to tow hard-body decoys stably on towlines,
at speeds from very subsonic to low supersonic. The answers are not what one would
expect, based on the towed gunnery
targets that have been flown for some decades now. Straight tow is the easiest to achieve at all
speeds, meaning the tow line extends mostly
straight back from the aircraft,
although you DO NOT tow the body by its nose! Low or high tow are
far, far more difficult to achieve, especially as speeds become high subsonic and
the aero forces exceed the weight force.
Stable side tow is nearly impossible,
even at low subsonic. This
applies to radar decoys as well as IR decoys.
Exploring how to tow hard bodies behind aircraft might be
the topic of a future article or articles,
or even part of a book. The basic
rules were invented by my friend Byron Hinderer. I researched the details, and documented what did not work, as well as what did, in the wind tunnel while at Tracor.
The final unaddressed topic deals with what is called “engagement
analysis”, where the geometry of
the aircraft, the tow, the approach geometry of the attacking
aircraft or missile, and the
characteristics of the decoy (IR or radar) and the seeker, all interplay. The desired result is an estimate of the kill
probability for the attack. The decoy
designer wishes to reduce that kill probability to near zero.
Exploring engagement analysis with IR decoys and IR threats
might be some future article. Or it
might also be part of a book on these experiences. This topic I learned and practiced while at
Tracor.
Update 4-7-2024: added 3 to rocket, below.
Update 3-6-2024: added 3 to rocket, below.
Update 2-13-2024: added 1 to ramjet and 6 to rocket, etc. below.
Update 10-1-2023: added "Basic Thermal Results for High Speeds" to 2 topics below.
Update 9-2-2023: added "Purported SR-72 Propulsion" to 3 topics below.
Update 7-18-2023: added 1 article to forensics.
Update 6-21-2023: added 2 articles to rocket ballistics and vehicle performance list.
Update 5-4-2023: added 1 article each to aerothermo and forensics lists.
Update 2-4-23: added new nozzles article to aerothermo and ballistics lists.
Update 1-1-23: added catalog topic for towed decoys, this text color.
Update 12-2-2022: two ramjet articles added to that topic list, this color.
Update 9-5-2022: some recent articles added to the lists, this text color.
Update 10-1-2022: some others added, this color.
Update 10-30-2022: a couple added, this color.
------------------------------
I was once an all-around ramjet design, development, and test engineer, among many other things, including rocket work. This was mostly at a plant in McGregor, Texas, once known as Rocketdyne or Hercules. Part of that reservation is where SpaceX tests rockets now.
I did just about everything there was to do, for this ramjet work. There are very few indeed with knowledge and experience this comprehensive, I was definitely not a narrow specialist! But my knowledge and abilities, in each of all these different specialty disciplines, was actually quite substantial and deep!
My design analyses usually took
the form of custom hand-calculations, not just sitting
there blindly running other people’s computer codes. (Although, I did use computer
codes, and even wrote some myself.) I have informally published several
articles on my blog site that describe how some of this ramjet work was done.
Ramjet & Closely-Related Articles (there are
others, but these are the best):
2-13-2024 GW's Ramjet Book Is Now Available
10-1-2023 Basic Thermal Results for High Speeds
9-1-2023 Purported SR-72 Propulsion
12-2-2022 The Unchoked Gas Generator As A Throttle For Gas Generator-Fed Ramjets
12-1-2022 How Ramjets Work
10-30-22 Plasma Sheath Effects in High Hypersonic Flight
6-1-22 About Hypersonic Vehicles
11-2-21 The “Warm Brick” Ramjet Device (nonpropulsive
application to an infrared decoy) [also the 11-2-21 update to this catalogue list]
10-1-21 Use of the Choked Pintle Valve for a Solid Propellant
Gas Generator Throttle
8-2-21 The Ramjet I Worked On the Most
7-1-21 Another Ramjet I Worked On
11-9-20 Fundamentals of Inlets
3-3-20 Ramjet Flameholding
2-16-20 Solid Rocket Analysis (applies to ramjet for
boosters)
2-4-20 One of Several Ramjets That I Worked On
1-2-20 On High-Speed Aerodynamics and Heat Transfer
11-12-18 How Propulsion Nozzles Work
7-4-17 Heat Protection Is the Key to Hypersonic Flight
6-12-17 Shock Impingement Heating Is Very Dangerous
12-10-16 Primer on Ramjets
12-21-12 Ramjet
Cycle Analyses
These are located on http://exrocketman.blogspot.com, along with many others on a wide variety of
subjects.
There is a navigation tool on the left of that page. For the article you want, you only need its publication date and its
title. Use the navigation tool: click on the year, then the month. Then click on the title if you need to. The data you need are in these lists.
If you click on one of the figures, you can see all of them enlarged. You see nothing but the figures, though.
There is an “X-out” from this view,
upper right of screen.
At the end of any given article, there is also a list of search keywords
assigned to it. If you click on
“ramjet”, you will only see the articles
bearing that keyword. The same is true
of the other keywords.
Here follows a photo of one of the ramjets I worked on: ASALM-PTV. It is hanging under the wing of an A-7 Corsair-II, an aircraft my father designed. I always considered this photo a sort of “family portrait”.
ASALM-PTV Ramjet Vehicle Underwing of A-7 Corsair-II
Some of those ramjet articles overlap with the next
list. That next list is of
aerothermodynamics and heat transfer-related articles. Some of these relate to high-speed
atmospheric flight, and others to
atmospheric entry from space. Those two
scenarios are quite different, in that
atmospheric flight is a steady-state equilibrium problem, while atmospheric entry is mostly a transient
heat-sinking problem. The search keyword
for these is “aerothermo”. Clearly, I was adept at multiple specialties.
Aerothermodynamics & Heat Transfer Articles:
1-2-2024 Airplanes on Mars?
12-9-2023 Overall Study Results: Propellant From Moon
11-22-2023 How the Suborbital "Hopper" Calculations Were Made and With What
11-21-2023 Upgraded Rocket Hopper As Orbit Taxi
11-4-2023 Surface Freight Transport On Mars (not actually rocket, but related)
11-1-2023 Rocket Hopper For Mars Planetary Transportation
10-1-2023 Basic Thermal Results for High Speeds
9-1-2023 Purported SR-72 Propulsion
5-1-23 Heat Shields
2-4-23 Rocket Nozzle Types (bells and aerospikes)
9-18-22 Plasma Sheath Effects in Hypersonic Flight
7-3-22 Early High-Speed Experimental Planes
6-1-22 About Hypersonic Vehicles
4-1-20 Entry Heating Estimates
1-2-20 On High-Speed Aerodynamics and Heat Transfer
1-9-19 Subsonic Inlet Duct Investigation
1-6-19 A Look At Nosetips (Or Leading Edges)
1-2-19 Thermal Protection Trends For High-Speed
Atmospheric Flight
11-12-18 How Propulsion Nozzles Work
7-4-17 Heat Protection Is the Key to Hypersonic Flight
6-12-17 Shock Impingement Heating Is Very Dangerous
11-17-15 Why Air Is Hot When You Fly Fast
8-4-13 Entry Issues
3-18-13 Low-Density Non-Ablative Ceramic Heat Shields
1-21-13 BOE Entry Analysis of Apollo Returning From the Moon
1-21-13 BOE Entry Model User’s Guide
8-19-12 Ballute Drag Data
8-19-12 Blunt Capsule Drag Data
7-14-12 “Back
Of the Envelope” Entry Model
I was also a rocket propulsion engineer, mostly in solid composite propellants. However,
from the chamber outlet through the nozzle, the ballistics of all rockets are the
same, including liquid propellant
rockets. If you can allow for any gas
bled off and dumped overboard for turbopump operation, then the very same ballistics apply, right down to the chamber pressure vs flow
rate calculation.
Further, the
estimation of vehicle performance from the simple rocket equation can be made
quite accurate, if you know how to apply
“jigger factors” in the appropriate places for gravity and drag losses, and if you know what values of these “jigger
factors” to apply. I have been very
successful at doing this kind of work. The following list shows that, and mostly shares the “launch” and “space
program” keywords. While still a graduate student, I spent a summer doing advanced configuration and mission work at what was then LTV Aerospace, working on its "Scout" 4-stage solid satellite launcher.
Rocket Ballistics and Rocket Vehicle Performance
articles:
4-4-2024 Ascent Compromise Design Trade Study
4-3-2024 Bounding Analyses for TSTO
4-2-2024 Bounding Calculations for SSTO Concepts
2-25-2024 Tricky Landing
3-3-2024 Launch to Low Earth Orbit: 1 or 2 Stages?
3-4-2024 Launch to Low Earth Orbit: Fixed Geometry Options
9-1-2023 Purported SR-72 Propulsion
6-20-23 TSTO Launch Fundamentals
6-6-23 Frontal Thrust Density In Rockets
2-4-23 Rocket Nozzle Types (bells and aerospikes)
10-27-22 Getting to Low Earth Orbit (vertical ballistic launch versus lifting ascent)
10-1-22 Rocket Engine Calculations (how to rough-out or reverse-engineer, ex: Raptor-2)
9-7-22 Two-Stage Reusable Spaceplane Rough-Size (VTO HL both stages)
8-4-22 Engineering Lander/Rover for Mars
5-1-22 Investigation: "Big Ship" Propellant From the Moon vs From Earth (added to list as part of Update 5-1-22)
4-2-22 Earth-Mars Orbit-to-Orbit Transport Propulsion Studies (added to list as part of Update 5-1-22)
2-1-22 A Concept for an On-Orbit Propellant Depot
8-18-21 Propellant Ullage Problem and Solutions
3-15-21 Reverse
Engineering Estimates: Starship Lunar Landings
3-9-21 Reverse-Engineering
Starship/Superheavy 2021
3-5-21 Fundamentals
of Elliptic Orbits (delta-vee requirements)
2-9-21 Rocket Vehicle Performance
Spreadsheet (rocket vehicle performance)
7-13-20 Non-Direct to the Moon
with 2020 Starship
7-5-20 How the Spreadsheet Works
(Starship to Mars)
7-5-20 2020 Starship/Superheavy
Estimates for the Moon
7-3-20 Cis-Lunar Orbits and
Requirements
6-21-20 2020 Starship/Superheavy
Estimates for Mars
5-25-20 2020 Reverse Engineering
Estimates for Starship/Superheavy
2-16-20 Solid Rocket Analysis (solid ballistics & more)
11-21-19 Interplanetary Trajectories and
Requirements
10-22-19 Reverse-Engineering the 2019
Version of The Spacex “Starship” / “Super Heavy” Design
9-26-19 Reverse-Engineered “Raptor”
Engine Performance (liquid ballistics)
9-16-19 Spacex
“Starship” as a Ferry for Colonization Ships
9-9-19 Colonization
Ship Study
11-12-18 How Propulsion Nozzles Work (rocket, ramjet, & turbine; plain & free-expansion)
9-11-18 Velocity Requirements for Mars
8-23-18 Back-of-the-Envelope Rocket
Propulsion Analysis
4-17-18 Reverse Engineering the 2017
Version of the Spacex BFR
10-23-17 Reverse-Engineering the ITS/Second
Stage Of the Spacex BFR/ITS System
3-18-17 Bounding Analysis for Lunar
Lander Designs
3-6-17 Reverse-Engineered “Dragon”
Data
8-31-13 Reusable Chemical Mars Landing
Boats Are Feasible
In 2009, I attended
an asteroid defense conference in Granada,
Spain, as a poster paper
presenter. I have since written some
articles about asteroid defense.
Unfortunately, the asteroid defense
capability picture hasn’t changed much since my 2009 attendance at that
conference. Again, the latest are the best and most up-to-date. Be aware that “NEO” (Near Earth Object) includes
comets as well as asteroids as threats. Comets may be the more difficult to defend against, because of the surprise nature of the detection and orbits. These articles all share the “asteroid defense” keyword.
Asteroid Defense Articles:
8-30-20 Asteroid Threats (current status assessment: not good)
6-3-20 On the Manned Spacex Launch
7-14-19 Just Mooning Around (asteroids plus Mars)
12-13-13 Mars Mission Study 2013 (what takes you to Mars takes you to asteroids)
4-21-09 On Asteroid Defense and a Good Reason for
Having National Space Programs
I have also applied my wide-ranging knowledge to the problems of
atmospheres to breathe while in space,
and the kinds of spacesuits that might best serve our needs. Again,
the latest is the best and most up-to-date. But I have been looking into these issues for
some time, as indicated by the dates on
these articles. These all share the
“spacesuit” keyword.
Space Suits and Atmospheres Articles:
1-2-22 Refining Proposed Suit and Habitat Atmospheres (update 1-2-22) best case and easiest-to-remember cases, plus an independent estimate of the utter min suit pressures feasible
1-1-22 Habitat Atmospheres and Long-Term Health (update 1-1-22) adds a long term hypoxia criterion for the habitat in addition to short term criteria for the min-P suit
3-16-18 Suit and Habitat Atmospheres 2018
11-23-17 A Better Version of the MCP Spacesuit?
2-15-16 Suits and Atmospheres for Space
1-15-16 Astronaut Facing
Drowning Points Out Need for Better Space Suit
11-17-14 Space Suit and Habitat Atmospheres
2-11-14 On-Orbit Repair and Assembly Facility
12-13-13 Mars Mission Study 2013
1-21-11 Fundamental Design Criteria for Alternative
Space Suit Approaches
One of my
favorites is the MCP (mechanical counter pressure) version of the
spacesuit. This was pioneered by Dr.
Webb in the 1960’s as a possible suit for the Apollo missions to the moon. It is not a full pressure suit at all, but essentially a tight garment that simply
squeezes the body. It is porous, so that you sweat right through it to
cool, just like ordinary street
clothing. But this design was tested quite
successfully in 1968 for 30 minutes in a vacuum chamber, at way above the equivalent “vacuum
deathpoint” altitude. Photo follows:
Webb’s MCP Space
Suit: Helmet, Backpack,
and Supple Garment Total 85 Lbs
The reason why I like this approach over Dava Newman's designs is that Webb's designs are essentially vacuum-protective underwear that can be easily laundered. Over them you wear whatever unpressurized clothing you need for protection from from heat, cold, and mechanical hazards. All of these are separate, easily laundered items. I think the "one garment that does everything" approach, that we have been using since about 1960, is wrong. "Mix and match" is way more flexible.
Besides vacuum
death and microgravity disease, there is
also a radiation hazard to worry about in space. But,
it is not quite what you think:
there are two completely different hazards to worry about. On Earth,
we have two kinds of protection:
the atmosphere, and the magnetic
field. In low Earth orbit, we have only the magnetic field. Outside the magnetic field, going to the moon or anywhere else, there is no protection. Yet these things can be quantified, and some of it shielded fairly effectively. What got me started on this topic were the
dangers posed by the nuclear disaster in Fukushima, Japan. Keyword “radiation”.
NASA has since lowered its career exposure limits below the older values I had obtained from them. That avoids the slight chance of cancer late in life due to galactic cosmic ray exposure over long times in space. But, it makes passive shielding design bulkier, heavier, and more difficult to design. It's really a trade-off. However, NASA still has not faced up to the erratic but intense floods of radiation from solar eruptions. They haven't yet killed a crew from this, although they came close to that during Apollo. But if they don't address this, they will kill a crew, once we move out beyond the Van Allen belts, and try to stay there. That includes the return to the moon.
Radiation Hazard
Articles:
10-5-18 Space Radiation
Risks: GCR vs SFE
4-11-15 Radiation
Risks for Mars Trip
5-2-12 Space Travel Radiation Risks
3-24-11 Radiation and Humans
3-17-11 Follow-Up On the Japan Nuclear
Crisis
3-15-11 On the Nuclear Crisis In Japan
On a lighter note, I have
long been interested in pulsejet engines,
especially valveless pulsejets.
While teaching math at TSTC, Waco, I
became involved with mentoring a student who was also interested in
pulsejets. I and a colleague assisted
this student in making his own valveless pulsejet engines, which attention and involvement also turned
this student into an “A” student in math!
Keyword “pulsejet”.
That student built a small engine that eventually pushed an old golf
cart around, and then a much bigger
engine which we together fired up out here on my farm homestead. Photos of the two engines follow:
Smaller Student-Built Valveless Pulsejet Engine (Later Pushed a
Golf Cart)
Larger Student-Built Valveless Pulsejet Engine
Pulsejet Articles:
5-20-12 Recommended Broad
Design Guidelines For Valveless Pulsejet Combustors
4-30-12 Big Student
Pulsejet an Even Larger Hit at TSTC
3-6-12 Student
Pulsejet a Hit at EAA Meeting
11-12-11 Student Pulsejet Project
I have been interested in ethanol fuels since my early days
in college. When I went to work for what
is now Minnesota State University, after
my 20-year career in aerospace defense work ended, I got more serious about it. My next job was at Baylor University in
Waco, Texas, and it dealt directly in alternative fuels
for aircraft. The scope of that included
ethanol (and an ether) as piston-engine fuels,
and biodiesel-jet fuel blends as turbine fuels, plus STC work with the FAA, and also experimental engineering research
work, as well as classroom
teaching.
Not too long after leaving Baylor, I began my own experimental engineering
research at home, using E-85 ethanol
fuel, and stiff ethanol blends, in a variety of vehicles. Those would include straight E-85 ethanol
fuel in an old farm tractor and in an old-time air-cooled VW beetle, plus stiff ethanol blends in a variety of
completely-unmodified cars and 4-stroke lawn and garden equipment. I basically recommend up to E-35 blend
strength, as a “drop-in” fuel, for just about any 4-stroke piston
engine.
The keywords are “ethanol” and “old cars” for most of these
articles. Once again, the latest is the best and most up-to-date.
Articles About Ethanol and Ethanol Blends in Vehicles:
9-1-21 Making Stiff Blends At the Gas Pump
11-3-13 Aviation
Alternative Fuel Compatibility Issues
11-2-13 An Update on Ethanol Fuel Use
8-9-12 Biofuels in
General and Ethanol in Particular
5-4-12 Energy Storage: Batteries vs Unpressurized
Liquid Fuels
6-12-11 Another Red-Letter Day
5-5-11 Ethanol
Does Not Hurt Engines
2-12-11 “How-To” For Ethanol and Blend Vehicles
11-17-10 Nissan Mileage Results on Blends
11-12-10 Stiff Blend Effects in Gasoline Cars
12-15-09 Red Letter
Day: Ethanol VW Experiment Complete
7-1-09 Another
Antique Comes Out of Storage
I have returned part-time out of retirement to help a friend
with his auto repair business. I was
once ASE-certified as a condition of employment while teaching at Minnesota
State in its Automotive and Manufacturing Engineering Technology
department. Before that, I did most of my own automotive maintenance
and repair work. Accordingly, I have posted some articles about basic car
care, plus one funny. These all share the “old cars” and “fun
stuff” keywords.
I have since gone back into retirement. My friend now has a real mechanic, who knows more than I do, and is much more experienced, and faster.
Automotive Care Articles:
8-22-22 Automotive Work (another "funny")
3-4-22 Understanding Your Tires (added to this list as update 5-1-22)
12-3-20 Blinker Fluid (the “funny”, and it is a sight gag)
8-20-20 Underhood Check
7-25-20 Taking
Care of Car Batteries
When I returned to the rocket plant in McGregor for my
second employment there, the family and
I acquired an old farm outside McGregor as our home. We have been there ever since. This place was largely covered in shin- to
knee-high prickly pear cactus, so thick
there were few trails through it. After
grubbing it out of the house’s back yard with hand tools, I decided there had to be a better way to do
this cactus eradication.
I tried a variety of mechanical drags behind my old farm
tractor for some 15 years without success.
The results were always the same:
it looked better for a while, but
returned worse than ever before, within
months. My neighbor was trying shredding
at 1 inch off the ground. Eventually
that worked, but required the neighbor
to be out there shredding, every single
day, the same ground over and over, for 6 (or more) years. The neighbor also tried spraying herbicides
on one patch of ground, which took 3
years to show results, but then totally
reinfested within another 2 years.
I then tried to build a “scooper-upper” out of scrap
steel. The idea was to bust the
aboveground cactus loose from its roots,
and catch it on a tarp towed behind the “scoop-upper”, for disposal in a burn pit. It completely failed to work, because when the tool hit the cactus and
busted it loose from its roots, it fell
forward in front of the tool, instead of
backward onto the deck. The tool then just
ran over the top of the cactus debris. I
gave up in disgust when this failure-to-scoop happened.
I went back up a few months later to salvage the steel, and saw something totally unexpected: the cactus was dead and gone wherever the
tool had been towed! Grass was growing in
the cow pasture where the cactus had been.
It did not take very long to understand that the aboveground cactus
foliage had been crushed and damaged passing underneath the heavy tool, such that the pads dried out and died, before they could put down new roots from the
thorn sites in contact with soil. They
had completely composted away over those months.
I “played” with this tool to get it just “right”, and started killing acres of prickly pear
quite effectively, and with very little
time and effort involved. In fact, I still have this very same experimental
prototype, and it still works today. This prototype led to me filing a patent on
the cactus tool in 2002.
I revised the design to something more producible from real
steel stocks, and built two production
prototypes that worked just as well as the original experimental prototype, but were easier to build. Then,
with the patent in hand as of 2004,
I began building and selling these tools to the public. My first customer wouldn’t wait for a real
production tool, and insisted on buying
one of the two production prototypes. I
still have the other one. I still use
it, and it now serves as an experimental
test bed for new features, too.
As time went by, it
quickly became apparent that other folks had rockier land, or land with tree stumps. I changed the design twice, to add a heavier stabilizing snout, plus a “barge front” wedging surface to get
over small rock outcrops. This was quite
successful, and is embodied in the tools
still built and sold today.
A close friend wanted to do cactus-killing for hire, and bought a “one-off” design from me. I also helped him build and modify a few more
tools, until the “commercial version”
was defined: a really tough snout, a big “barge front”, and retractable wheels to facilitate stepping
over obstacles, plus easier loading up
ramps onto trailers.
When that friend retired,
I revised his “commercial” design into something that used a common core
tool chassis with my “homeowner grade” plain tool. This common core chassis had the big barge
front, and used either a tough snout for
the “plain tool”, or a longer tough
snout for the “hydraulic tool”, that was
also fitted with retractable wheels operated hydraulically. I sell both versions to this very day. Both are towed on a chain bridle behind a
farm tractor’s drawbar.
I am working on a third version that could be an alternative
implement affixed to the hydraulic boom of a skid-steer loader. It uses an already-available “universal”
adapter plate to accomplish this, as a
quick-change item. There is nothing to
report here yet about that project, but
the “plain” and “hydraulic” tools are well-described in a series of articles on
“exrocketman” under the keyword “cactus-killing”.
These two versions are shown in the photo, with the plain tool in the foreground, and the hydraulic tool in the background.
Foreground: Plain
Tool; Background: Hydraulic (Wheeled) Tool
The new skid-steer version has been tested and revised to a form that not only works, but is more easily manufacturable. It is now patent pending.
Articles Related to Cactus Eradication:
2-9-17 Time Lapse Proof It Works
7-30-15 New Cactus Tool Website
1-8-15 Kactus Kicker Development
1-8-14 Kactus Kicker:
Recent Progress
10-12-13 Construction of the Plain Cactus Tool
5-19-13 Loading Steel Safely (Cactus Tool)
12-19-12 Using the Cactus Tool or Tools
11-1-12 About the Kactus Kicker
12-28-11 Latest Production Version of the Kactus Kicker
7-7-23 On the loss of the "Titan" Submersible (added 7-18-23)
4-25-23 Starship/Superheavy Flight Test
12-1-21 The Seal Failure in the SRB That
Doomed Challenger
12-10-20 Spacex Test Flight Results
in Explosion
9-1-20 On
the Beirut Explosion
5-4-18 Some Thoughts on the Anniversary of the West
Explosion
11-1-14 Two Commercial
Spaceflight Disasters in One Week
7-9-13 On
the Asiana 214 Crash
7-9-13 On
the Train Wreck in Quebec
4-18-13 Fertilizer
Explosion in West, Texas
9-23-11 Air Races, Air Shows,
and Risks
6-3-10 Plenty of Blame to Go Around for the Disaster
in the Gulf
5-20-10 It really was the North Koreans who sank the South Korean ship
Update 1-1-23: these are the articles related to towed decoys:
Between my tenures at the McGregor rocket shop, I worked at what was then Tracor Aerospace in
Austin, Texas, doing aircraft and ICBM countermeasures
work. The bulk of this related to towed
aircraft decoys, which are more advanced
aircraft countermeasures against missiles than the traditional chaff and
flares. I did all sorts of lab, wind tunnel,
and flight tests with these things.
To a great extent, I had to
design my own tests, test hardware, and equipment, too.
Tracor Austin became part of British Aerospace after I left
to go back to the rocket shop in McGregor,
and it closed entirely, only
somewhat later. When you combine the
typical corporate management misbehavior with the massive defense industry
contraction that happened after the fall of the Soviet Union, this plant closure outcome is entirely
unsurprising. That was as true for the
rocket shop as well as for Tracor. And
it is why I had to leave the aerospace defense industry entirely, after being laid off in late 1994 due to the rocket
plant closure in McGregor.
My work at Tracor in towed aircraft decoys related to two
distinct types of decoys: towed hard
body decoys, and towed ribbons. The hard bodies are exactly that: some sort of small airframe towed behind the
aircraft that it is intended to protect,
on some sort of towline. These
could be radar (RF) decoys to replace chaff,
or they could be infrared (IR) decoys to replace flares and
jammers. I worked on both of these towed
decoy types (RF and IR). Towed RF decoys
are now operational with the air forces of multiple nations, because they really work.
The towed ribbon decoys are quite different, being rather similar to windsocks and soft
towed gunnery targets. The technologies
supporting this concept apply only to RF,
and are restricted to only extreme-low observables aircraft. I also worked on these. One huge issue is stable tow for extended
periods of time, when the
“flapping-flag” effect wants to destroy them in mere seconds at jet aircraft
speeds.
Obviously,
deployment, especially very rapid
deployment, is another huge issue with
these ribbon decoys, as well as with the
hard body decoys. Solving it requires expertise in dynamics as well as
aerodynamics, plus knowledge of all
sorts of mechanisms.
Here is the list of my towed decoy articles available as of
this update. Future updates may add
more.
1-1-23 Towed Hardbody Decoys (could IR or RF)
11-2-21 The “Warm Brick” Ramjet Device (nonpropulsive application to an infrared decoy)
Later possible
articles on deployment and on towed ribbons