One of the most unusual ramjet projects I ever worked on was a non-propulsive device. This was a very miniature ram-fed airbreathing combustor, that was to be the hot gas generator for an infrared (IR) decoy. This decoy was to be towed behind an aircraft in lieu of a whole series of dispensed flares. It was intended to work by having enough IR output to cause the aircraft to drop out of the missile field-of-view first. See Figure 1 for that concept. I was working for my friend Byron Hinderer doing this.
Figure 1 – Towed IR
Decoy Concept, called “Warm Brick” at
Tracor in 1984
I did this at what was then Tracor Aerospace, in Austin,
Texas, during 1984. We called this decoy “Warm Brick”, and my job was to determine if this concept
was even feasible (it was). Our idea was to
heat a porous refractory material until it glowed brightly in the IR. We preferred fuel-air combustion to minimize
decoy mass, and ram combustion is the
simplest of the airbreathers. Plus, I had lots of experience with ramjet
combustion at what was then Rocketdyne/Hercules in McGregor, Texas.
To the very best of my knowledge, no patent was ever taken out on this
concept, and Tracor never did anything
at all with it. Even if there had been a
patent, and it had been
renewed, any such patent would have
run out by now. So, what I reveal here should offend no one, and infringe no patents.
As implemented for the feasibility tests, this concept took the form of a “gasoline
lantern mantle” made out of commercial ceramic fire curtain cloth, as the IR emitter. This was to be mounted behind a wake-producing
spoiler, mounted at the aft end of the
burner and inlet assembly. The decoy
might carry its own fuel tank, or it receive
fuel down its tow line, if a heavier tow
line could be tolerated.
To test the scientific and engineering feasibility, I designed a very generalized inlet and
burner hardware set that was flexible enough to allow evaluation with a variety
of gaseous and liquid fuels. See
Figures 2 and 3. The intended
flight conditions were relatively low altitude from mild subsonic to
barely-supersonic speeds, typical of an
attack aircraft threatened by surface-to-air missiles.
Figure 2 – Assembly
Sketch for the Initial Version “Warm Brick” Ram Combustor Test Device
The assembly sketch clearly depicts the long fuel
injection-and-mixing duct allowed between the inlet diffuser and the sudden
dump into the combustor. There was an
inlet piece and a fuel injector piece,
both made of aluminum for ease of rework, and an inlet tube and a combustor shell, both made of steel. The combustor shell was sized for fabrication
from 2-inch schedule-40 pipe, but ended
up being made of 300-series stainless to those same dimensions. We tried automotive-style spark ignition.
One can easily see how the molded low-density ceramic liner
insert was to be trapped in place by the nozzle block. The arrangement shown in the assembly sketch of
Figure 2 (directly-pinned nozzle block) was quickly replaced by a pinned steel
nozzle shell ring, as shown in the
hardware photo (Figure 3). This revision
happened about the same time that the first (unreinforced) liner was replaced
with the second liner (reinforced ceramic composite).
Figure 3 – Photo of
the “Warm Brick” Ram Combustor Test Hardware as Revised
The design concept called for a small combustor fed by a
simple pitot inlet, with a convergent-only
nozzle that would likely function unchoked at most conditions. I chose a center-duct coaxial air entry with
sudden-dump flame stabilization, similar
to the successfully-flown ASALM-PTV liquid-fueled ramjet test vehicle. Geometric
ratios were initially set equal to those used in ASALM.
Based on Reference 1, I chose a minimum ¼-inch (6 mm) step height
around the dump. The combustor length
was sized “empirically” (rules of thumb based on ASALM-PTV geometry) so that
the annular separation bubbles would close,
and the axial core would be “burned out”, before any of these flows entered the nozzle. That was basically an assumed 11-degree
spreading angle, on both sides of the
mixing layer between the entering mixture and the recirculated flame. That’s
too crude, in hindsight.
We wanted sufficient porosity in the emitter so that the
burner operation would be unaffected by the presence or absence of the emitter. The fire curtain cloth gave us that, in the sizes tested, because the surface area of the ellipsoidal
shape was so large relative to the final burner throat area. Its effective porosity-driven “free” open
area was very much larger than any of the burner throat areas we tested.
There were two crucial unanswered questions: (1) emitter/hot gas coupling (could we
really get the emitter hot enough to radiate effectively?), and (2) obtaining stable combustion at all
in a burner that small, with any fuel
whatsoever! There was an extensive paper
trade study done, to determine the desired
fuels. In test, these fuels,
and some other fuels that were easier to use, were investigated.
This combustor was nominally 1.5 inch (38 mm) inside
diameter, as insulated, and 3 inches (76 mm) long inside. The smallest size ramjet combustor in my
experience up to that point had been some heavyweight solid-propellant ducted
rocket ramjet work (in a completely-different geometry) at 4.6 inch (117 mm)
inside diameter, and length/diameter
6-to-8. The largest was ASALM-PTV at a
20 inch (51 cm) combustor case diameter.
“Warm Brick” was smaller than anything of which I had any knowledge!
I didn’t want to periodically replace an ablative liner in
the test burner, and I didn’t want to
attempt an air-cooled liner shell for full-rich combustion in something that
small. So I opted for an unknown, inspired by the Space Shuttle’s heat shield tiles. Could I put a low-density ceramic insulator
in this combustor, and not melt it? The answer turned out to be “yes”, but it took some adaptive effort.
The project operated in three logical parts: (1) obtain stable combustion with a variety
of fuels in the burner alone, (2) add
the emitter and determine how best to shape,
fabricate, and attach it, and (3) document infrared radiometric
output. The real prerequisite for part
(1) was the combustor insulator, since
we started with gaseous fuels, thereby
avoiding the fuel vaporization issue.
I selected free-jet test mode as the best way to accomplish all three parts of
this project with the same hardware and test setup (see
Figure 4). All that I had
personally done while at Rocketdyne/Hercules was direct-connect testing, but I knew about free-jet testing, both from my research, and some experimental association with
Marquardt, while I was with
Rocketdyne/Hercules.
We used a commercially-rented air compressor trailer as our
air source, to be run real-time. In 1984,
this 750 SCFM unit was the largest of its kind in Texas. It fed a PVC pipe stilling chamber, terminating in a simple convergent-only
nozzle block made (conveniently) of wood.
Figure 4 – Test
Setup: Stilling Chamber Exhausting To Left, Fed From Right
The test article was bolted to a heavy pipe
stand-and-sting, with its inlet immersed
in the free jet of air. That free jet
typically measured 190 F (88 C) stagnation temperature, at full-power compression conditions.
The first part of the investigation began with bottled
hydrogen gas fuel (series 1). This and
all the other trials are summarized in Table 1 below. Series 1 wasn’t very successful for two
reasons: (1) the nozzle was too wide
open for a stable flame, and (2) free
jet air speeds higher than about 0.25 Mach blew the spark column out from the
electrodes of the spark plug, even
though it was located flush within the annular recirculation zone.
The device didn’t ignite at all until I obstructed the
nozzle with a scrap of wood, and it still
went out after ignition, if I removed
the obstruction. So, I built a smaller-throat nozzle block. We still had to ignite at low airspeed and gradually
work up to higher speeds, limited at
that time to about half a Mach number by the stilling chamber nozzle. I also tried liquid ethanol unsuccessfully at
this time (series 2).
Somewhere in all of this,
I first drove the combustor into what proved to be a very
violent rich blowout instability,
and completely shattered my first (unreinforced) liner! The combustor visibly shook on its
sting, and it spit the pieces of its
liner out the nozzle, igniting a local
grass fire! Later, we estimated a pressure amplitude near 0.8
atm, at audio frequencies (a few hundred
Hertz), for this instability.
A photo of the liner molding tools that I used is given
in Figure 5, which includes the
basic combustor shell as the outer forming tool for the combustor liner. Both it and the nozzle block were laid up as
(commercial) low-density molding compound troweled onto the wooden plug, and inserted into the corresponding shell for
cure. I used Cotronics Corp. 360M low-density
molding compound for this.
Figure 5 – Tools Used
for Molding Ceramic Combustor Insulation Liner Inserts
These parts were cured at 215 F (102 C) in an oven to drive
off the water. The circuitous paths for
exiting steam led to a low density ceramic matrix. The resulting parts were coated with a
paint-like ceramic cement (Cotronics Corp. 901), and cured again, in the same oven. The unreinforced liner showed evidence of hot
gas flow behind the insulation, and into
the cracks, shown in Figures 6 and
7.
Figure 6 – Recovered
Pieces of Shattered Unreinforced Liner,
Bonded Together
Figure 7 – View of
Fracture Surface, Showing Hot Gas Flow
Damage with Sooting
I built a second ceramic composite liner reinforced
by layers of the fire curtain cloth (woven from 3M Nextel 312), which survived all instabilities and any
other test abuses thereafter. It
survived many hours of accumulated burn time in near-pristine condition, as seen in Figures 8 and 9. The shrinkage cracks did not preclude
functionality. There was some melting evident
in the throat of the nozzle.
Figure 8 – View Into
Near-Pristine Reinforced Liner, After
Hours of Burn Time
Figure 9 – View Into
Reinforced Nozzle Block, After Hours of
Burn Time
Once we had the burner working at all, we tried some test sample pyrometers in its
exhaust plume, with both propane and
acetone as fuel (series 3, and acetone
proved worthless as a fuel). These pyrometers
would be old nails, or else planar
samples of potential emitter materials.
We even tried gasoline as fuel (series 4), but results were poor, and it became very obvious that poor
vaporization was the cause! I tried propane
again (series 5) as the most successful fuel,
and got enough radiometer output to be encouraging, from a sample of the fire curtain cloth
immersed in the jet exhaust.
So, I created a
fuel-line hot-soak bucket to correct the poor fuel vaporization problem for
test purposes. This took the form of an
electrically-heated bucket of old motor oil,
in which a coil of the fuel supply line was immersed. That rig is shown in Figure 10. It may resemble a moonshine
still, but it is not!
Figure 10 – Fuel
Vaporization Preheat Bucket Rig
At this point, I had
a crudely-successful burner, but an
unproven fuel supply method. I checked
out the combined burner and fuel vaporization bucket, first on propane (series 6), then on aviation gasoline (series 7), and finally on a “home-made version of JP-4” that was actually half Jet-A and half
aviation gasoline (series 8). Plus, I added instrumentation to the burner unit
(enough manometer pressures and thermocouples to attempt an actual “engine” cycle
analysis).
Results, including the
exhaust pyrometer samples, were
favorable enough to warrant continuing the project further. It still required a lower-airspeed
ignition. I stood in the jet blast for
all these tests, looking directly into
the flame zone, and sniffing for unburned
fuel, to set mixture. That “settled” the fuel injection and
ignition issues well enough to test emitter coupling issues for the very first
time.
The first actual emitter was made of Nextel 312 fire curtain
cloth, coated with the Cotronics 901 adhesive
as a “paint”. It was sewn together, with alumino-silicate thread, from bias-cut gores much like a balloon, to form an elongated semi-ellipse
approximation. The seams were left on
the outside of this first emitter, as
shown in Figure 11. It was the
first of several series 9 tests with pre-heated propane, at air speeds up to about Mach 0.47. Those test conditions are depicted in
Figure 12.
Figure 11 – Test
Setup for First-Article Emitter
For all subsequent tests,
the seams in the sewn emitters were placed to the inside, as is depicted in Figure 13. That photo shows post-burn appearance of two
series 12 emitters tested with ethanol fuel,
but all the internal-seam emitters appeared similar, regardless of series and fuel.
These articles were brittle and fragile post-test, as expected for alumino-silicate materials
soaked to temperatures exceeding the solid phase-change temperature of about
2350 F (1290 C). That fragility alone
confirmed a high surface temperature for radiation purposes! This was also verified by radiometric
measurement, which also indicated very “non-gray”
behavior, in that the effective color
temperature (radiation peak wavelength) was substantially cooler than the
actual temperature.
The spoiler just ahead of the emitter clamp mounting
provided protection from direct wind blast forces. Plus,
it also provided effective hot gas recirculation effects external to the
emitter surface. Both acted to raise
emitter material soak temperature, and
therefore IR output, quite successfully.
Figure 12 – Test
Conditions Explored with Series 9 Propane
Two tests were made as series 10 in this same configuration
with the “home-made JP-4” fuel. Results
were similar to the series 9 propane runs,
except for a small liquid-wet “cold spot” at the very end of the emitter
bulb. This was due to still-unvaporized
kerosene hitting the emitter on-axis.
Figure 13 – Post-Test
Emitter Appearance from Series 12 Ethanol Tests
Sometime during this checkout process before the series 9
propane runs, I successfully modified
the inlet to a larger lip radius, in order to decrease its “buzz” instability
tendencies at higher backpressures. That
also greatly improved ignition characteristics,
and it further pushed the rich blow-out instability limits to richer
mixtures! The test set-up for cold-flow
inlet calibration is shown in Figure 14.
Both the original and modified (larger lip radius) inlets
were cold-flow tested with this rig.
Data were cross-plotted in a variety of ways. The data plot format for “typical” supersonic
ramjets was rather undiscriminating at these subsonic speeds: stream tube area ratio versus Mach and
stagnation pressure recovery ratio versus Mach.
Plots in the more primitive-variable format were actually more useful
for this mostly-subsonic system. These
included the diffused Mach to freestream Mach ratio, and the static “pressure gain” ratio.
These results guided the 1984-vintage data reductions of the
series 9 propane runs with emitters.
From those, installed hot-burn
test inlet performance data matched the cold-flow tests. The streamtube area recovery ratio shows a
very strong influence of the so-called “highlight” area versus the true minimum
area, when used as the reference area for
the calculation.
After the fact, this was
entirely expected, based on Reference
2, which (of course) recommends
the highlight definition. At the time I
did these tests, I had used something
pretty close to the minimum area for the reference. It
shows explicitly in the data, as a
recovery ratio substantially greater than unity, which is completely out-of-line with the
usual expectations for ramjet inlets.
See Figures 15 and 16.
Figure 14 – Cold-Flow
Inlet Calibration Test Rig
After the series 9 and 10 tests, the air nozzle in the stilling chamber was
replaced with a second wooden unit of slightly smaller throat diameter, as depicted in Figure 17. This enabled free jets of nearly Mach 1 speed
at the maximum compressor output. Two
more test series were conducted with this change, specifically to obtain data at those higher
simulated air speeds. These were series
11, using both propane and hydrogen
fuels, and series 12, which used the finally-selected ethanol
fuel.
The series 12 tests employed both radiometer
measurements, and imaging with a thermal
imager camera. The fuel vaporizer rig
was less successful with a high latent heat pure-substance fuel (ethanol), than it had been with distillate fuels, or with the easily-vaporized propane. With ethanol,
it was essentially long-period unstable,
with an oscillating fuel flow output.
The cycling time was a few seconds.
Nevertheless, using
ethanol fuel produced an output spectral power distribution closer to what is
needed from the non-gray decoy. The radiometer
data clearly showed this. We attributed
this difference (with a high degree of confidence) to the lack of yellow carbon
glare in the ethanol flame. This yellow
carbon glare was quite noticeable in the propane tests, and even more so when using gasoline or jet
fuel. The series 12 ethanol runs looked to
the eye “positively white” in comparison.
The ethanol fuel injector was stopwatch-and-bucket
calibrated for those series 12 tests. Those calibration data are shown in
Figure 18.
Figure 15 –
Calibrated Inlet Performance Derived from Series 9 Data, Part 1
Figure 16 --
Calibrated Inlet Performance Derived from Series 9 Data, Part 2
Figure 17 – Air
Nozzle Re-Work for Higher-Airspeed Test Capability
Figure 18 – Flow
Calibration Data for the Series 12 Ethanol Fuel Runs
After these tests,
the fuel vaporization problem was conceptually addressed as a hot-gas
tap from the forward end of the combustor to the lower-pressure zone at the
minimum area of the inlet. Fuel would be
injected into this very hot recirculated gas stream to effect rapid
vaporization. While the design analysis
looked good, that concept never
received any testing due to budgetary constraints that essentially
stopped all experimental work on the project after late 1984. Some prototype flyable hardware was
designed, and a few of those parts
manufactured, before all work on the
project was completely stopped. It
never resumed. So NOTHING is
confirmed about any of this!
The ceramic liner material was never characterized, it “just worked”. Density,
strength, and thermal conductivity
were never measured in any way!
However, it handled as if it were
about as dense as commercial Styrofoam products. The strength was considerable, considering the rich blow-out instability
abuse it endured. Immersed in a 190 F
(88 C) air stream, the combustor shell
would “barely boil spit” after an hour-long burn test at full rich mixture
(theoretically around 3800 F or 2100 C),
with but 0.2 inch (5 mm) thickness of the insulation! That indicated very low thermal conductivity
indeed!
Table 1 – Summary of
“Warm Brick” Burner Tests
In recent years, I developed further those basic cycle analysis techniques applicable to a low-speed ramjet system, or a subsonic nonpropulsive item like “Warm Brick”. In particular, I programmed them into an “Excel” spreadsheet, and reanalyzed the “typical” series 9 propane run at 0.47 Mach air speed and full-rich mixture. The spreadsheet setup is shown in Figure 19, and the spreadsheet results in Figure 20. Since then, I have created a real low-speed ramjet cycle analysis code. It works just fine.
These recent compressible-flow cycle analysis results
defined the bulk flow conditions inside the combustor well enough to attempt a
heat transfer model with a reasonable expectation of success. That model was cylindrical convective-conductive, and based on standard compressible flow
models inside and outside the combustor shell.
Radiative loss was near zero, as
there was no effective path by which thermal radiation could leave the
interior. The shell radiation cooling potential
was very low.
While the steel shell has a well-known thermal conductivity, the ceramic composite liner did not, so I ran this model parametrically versus
conductivity values from “very low” to “very high”. The “best” value of thermal conductivity was
that which matched both my recollections of perceived shell temperature, and my observation that the liner
surface was often close to melting (3250 F, 1790 C).
Those thermal conductivity results are given in Figures
21 and 22. The highlighted value
of 0.02 BTU/hr-ft-F equates to 0.035 W/m-C.
Density and strength still lack actual characterization! I have often wondered whether this material
might serve as a re-entry heat shield material, the way that the somewhat-similar low-density
ceramic Shuttle tile did. But that is
another topic for another venue.
References:
#1. Curran, Edward
T., “An Investigation Of Flame Stability
In A Coaxial Dump Combustor” (dissertation,
AFAPL/RJ WPAFB, Dayton, OH),
AFIT/AE/DS 79-1, Jan. 1979.
#2. Seddon, J., and Goldsmith, E. L.,
“Intake Aerodynamics”, AIAA
Education Series, 1985, ISBN 0-930403-03-7.
Figure 19 –
Spreadsheet Setup for “Warm Brick” Cycle Analysis at Series 9 Propane
Conditions
Figure 20 –
Spreadsheet Cycle Analysis Results for “Warm Brick” at Series 9 Propane
Conditions
Figure 21 – Heat
Transfer Model Results for “Warm Brick” Liner Thermal Conductivity
Figure 22 – Heat
Transfer Model Results Plotted vs Radius
Epilogue: Some Practical Combustion Device Lessons
Learned
Cycle analysis with one-dimensional flow models turned out
to be less important than the actual scale-dependent physical chemistry of
flame stability, for this “Warm
Brick” device. Residence time is proportional to dimension, all else equal, while chemical reaction rates are
scale-independent. This alone suggests
there is a minimum size below which a thing “just won’t work” with a particular
fuel.
Mixing is another very strong determinant of flame
stability. Mixing is not proportional to
scale, nor is it scale-independent, but it is something in-between. Again,
this also suggests that there is a size below which a thing “just won’t
work” with any particular fuel. That is
precisely one issue (of many) in flameholding.
Those considerations explain why the required nozzle
contraction ratio (and internal flow velocities) were so low in the “Warm
Brick” device for stable ignition and burning,
relative to everything I knew about, before I attempted this project. However,
these experiences with the Warm Brick subminiature combustor predate the
in-depth understanding of flameholding and flame stability that I was later
able to achieve, after returning to
Rocketdyne/Hercules. That knowledge is
summarized in the “exrocketman” article titled “Ramjet Flameholding” (on this
site) and dated 3 March 2020.
The vaporization of fuels of different latent heats and
boiling behavior revealed a surge instability in the hot-bucket fuel rig
(referring again to the crude hardware in Fig. 10 above). The basic layout was a source of fuel at
pressure, led through a copper line
coiled in the hot bucket, and from there
to the metering orifices inside the test article. See the cartoon in Fig. 23.
The source of fuel-at-pressure was a standard 5-gallon
propane bottle (usually around 200-250 psig),
or a welding gas bottle (initially 2200 psig), or a pressure tank of liquid fuel pressurized
with compressed dry nitrogen (usually pressurized in the 100-300 psig range). All of these pressurization schemes are
regulator-controlled. That regulator was
physically located about 5-to-10 feet downstream of the test article, and within arm’s reach of the exhaust
plume. This allowed me to manually
adjust the fuel flow during the test by varying the regulated pressures, while standing immersed in the exhaust where
I could smell for unburned fuel. For the
open-nozzle tests, I could literally see
the flame up the tailpipe.
Fig. 23 – Conceptual Layout and Operation of Fuel Supply
When using hydrogen directly from the welding gas
bottle, there was no vaporization
problem, as this was simply compressed
hydrogen gas. We did not use a
pre-heater bucket with this fuel, but
the rest of the component layout in Fig. 22 is correct.
With propane in the 0.47 Mach air tests, we found the line just downstream of the
regulator, and the sides of the propane
bottle, to be cold. This is because the vaporizing pool of liquid
propane in the bottle must draw about 150 BTU/lbm of latent heat from itself
and from its surroundings, mostly
from itself (gets cold). If it
cannot draw sufficient heat to vaporize,
then it won’t vaporize, pressure
drop notwithstanding! The energy to
change phase (latent heat) simply must come from somewhere!
There was a cold-line risk of re-condensation on the way to
the test article, which we “cured” with
the hot oil bucket preheater. We kept
the line length from bottle to preheater as short as practical. We also found bottle “freeze-up” occurred at
the higher flow rates with the Mach 0.9 airstream tests. We “cured” that by the camper’s expedient of
putting the propane bottle in a tub of hot water.
With gasoline and jet fuel,
the driving pressures helped us pre-heat the liquid fuel without getting
any boiling in the fuel line. Without
preheat, there was insufficient air
stream heat in the test article to get the fuel to vaporize and burn. With about 300 F preheat, we got all but the “tag-end” of the
distillation curve to vaporize upon being injected, due to combined atomization and pressure-drop
boiling.
With the gasoline and 300 F preheat, our nominal 100-300 psig driving pressure was
apparently barely enough to prevent any significant boiling in the line, so we did not encounter any noticeable problems
with vapor lock-induced fuel flow rate surges.
With the jet fuel and its lower volatility, we had no real risk of vapor lock
surging, but we did see a little more
“tag end” unvaporized fuel, indicating a
higher preheat temperature was really needed.
Both of these are about 150 BTU/lbm latent heat materials.
We did have a real fuel surge problem running neat
ethanol as fuel. This material has a
far higher latent heat at about 378 BTU/lbm,
and it has a single normal boiling point, instead of distillation behavior. At our delivery conditions, the pressure was insufficient to prevent
boiling in the line, leading directly to
vapor lock-induced flow rate surging!
Fuel delivery rates oscillated through about a factor of two, on a long period of several seconds. It would vapor lock, unlock,
and relock to cause this surging.
We could not reduce preheat temperatures and still expect to
get any flash vaporization upon injection,
in hindsight due to that higher latent heat. We could not increase the feed pressures to
preclude the boiling without re-working the test article for much smaller
injection orifices. That latter is the real
design solution to this problem, but we
did not use it for these tests! We were
able to get our infrared radiometer data from the high points of the
oscillating-intensity burn.
While high pressure preheat to get flash vaporization from
an atomizing injector is an approach that really works, the equipment to do it is usually large and
heavy, too much so for a miniature decoy. The alternative would be to mix the fuel with
hot combustion gas to get vaporization,
downstream of the metering point.
The design difficulty is then to get good mixing of the fuel-rich gas stream
with the inlet airstream, without
suffering large pressure losses. That
seemed the better approach for the flight decoy design. We were never able to test this, though!
It is still just a concept!
For an aero-engine application, high-pressure fuel pre-heat with atomizing
flash vaporization is likely the better design approach. The sizing of required preheat depends upon raising
the liquid to a temperature such that the enthalpy drop across the injection
orifice exceeds the latent heat of vaporization. The size of the orifice and the feed line
pressure determine flow rate. But, the feed line pressures must always exceed
fuel vapor pressure at that high preheat temperature! If this is not done, then vapor lock-induced surging will occur, and at very significant magnitudes. Fuel control then becomes impossible.
As indicated, we
never got to test the concept of vaporization by injection into a hot combustion
gas stream, followed by injecting that
hot mixed stream into inlet air. There
is a lot of promise in that notion, but
it is fraught with practical difficulties,
as well.
Final Comments: IR
Emission Characteristics and Towed Decoy Physics
The IR emission characteristics topic has been
mostly ignored here, except to say these
ceramics were decidedly “non-gray” in their spectrally-dependent emissivity
properties. They were non-gray enough to
reduce expected radiation in the 1-2 micron band very markedly, to near what they emitted in the 3-5 micron
band, despite operating at a temperature
somewhere near 3000 F (1650 C). The effective
“color temperature” (really the wavelength at peak spectral distribution of
radiation) was much closer to typical tailpipe temperatures at full power (but less
than those with full afterburning).
Suffice it to say that a great deal of infrared power was
radiated by a very small object, whose
color temperature and radiated-power in-band looked like a very large jet
engine tailpipe at full power. This
little emitter would blister my face with radiated heat from some 20 feet
away. The large radiated power would be
the temperature-to-fourth-power effect,
while the color temperature would be the non-gray emissivity
effect. Both are critical effects.
Exploring this IR emission topic in more detail would be the
subject of some future article, or
perhaps even a book relating these experiences.
This is an application of otherwise well-established physics.
Another unaddressed topic is aeromechanical in nature: how
to tow hard-body decoys stably on towlines,
at speeds from very subsonic to low supersonic. The answers are not what one would
expect, based on the towed gunnery
targets that have been flown for some decades now. Straight tow is the easiest to achieve at all
speeds, meaning the tow line extends mostly
straight back from the aircraft,
although you DO NOT tow the body by its nose! Low or high tow are
far, far more difficult to achieve, especially as speeds become high subsonic and
the aero forces exceed the weight force.
Stable side tow is nearly impossible,
even at low subsonic. This
applies to radar decoys as well as IR decoys.
Exploring how to tow hard bodies behind aircraft might be
the topic of a future article or articles,
or even part of a book. The basic
rules were invented by my friend Byron Hinderer. I researched the details, and documented what did not work, as well as what did, in the wind tunnel while at Tracor.
The final unaddressed topic deals with what is called “engagement
analysis”, where the geometry of
the aircraft, the tow, the approach geometry of the attacking
aircraft or missile, and the
characteristics of the decoy (IR or radar) and the seeker, all interplay. The desired result is an estimate of the kill
probability for the attack. The decoy
designer wishes to reduce that kill probability to near zero.
Exploring engagement analysis with IR decoys and IR threats
might be some future article. Or it
might also be part of a book on these experiences. This topic I learned and practiced while at
Tracor.